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== Well Details == | == Well Details == | ||
− | {| class="wikitable" width="95%" | + | {| class="wikitable welldetails" width="95%" |
| Well ID: 37-059-25323 | | Well ID: 37-059-25323 | ||
− | | style=" | + | | style="height=100%; align=center" rowspan="14" | {{#display_map: 39.986475, -80.280627 | width=100% | height=100% }} |
|- | |- | ||
| County: [[Greene County, Pennsylvania|Greene]] | | County: [[Greene County, Pennsylvania|Greene]] |
Well ID: 37-059-25323 | Loading map...
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County: Greene | |
Municipality: Morris Township | |
Operator Name: CNX GAS CO LLC | |
Well Pad ID: 148000 | |
Farm/Lease Name: CONRHEIN NV26CV | |
First Permit Date: 2009-11-09 | |
Last Permit Date: 2009-11-09 | |
Spud Date: 2010-05-13 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: None | |
Latitude: 39.986475 | |
Longitude: -80.280627 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1910356 | 2010-09-01 | No Violations Noted | ||
1911295 | 2010-08-17 | No Violations Noted | Site Built and currently setting up the rig to begin drilling a Marcellus Well. | |
1917660 | 2010-08-24 | No Violations Noted | The Department was at the above referenced Marcellus Well to conduct a complaint inspection. The Operator is currently drilling multiple Marcellus Wells on this pad. The Department received a complaint in regards to the well site causing accelerated erosion on the down gradient property. The Department did observe E/S concerns at the site. The E/S controls need to be addressed. The water coming off the site has caused the valley to erode at a fast rate. The Department recommends installing a sediment trap and also turn-out ditches to slow down the water as a pollution prevention measure. The Department has spoke with the Operator and the land owner about the issues at the site. | |
1923864 | 2010-09-17 | No Violations Noted | The Department was at the above referenced Marcellus Well to conduct a complaint inspection. The Operator is currently drilling multiple Marcellus Wells on this pad. This is a follow-up to an earlier inspection on 8/24/10. The Department received a complaint in regards to the well site causing accelerated erosion on the down gradient property. The Department did observe E/S concerns at the site. The E/S controls need to be addressed. The water coming off the site has caused the valley to erode at a fast rate. The Department recommends installing a sediment trap and also turn-out ditches to slow down the water as a pollution prevention measure. The Department has spoke with the Operator and the land owner about the issues at the site. The Operator agreed to address the issues at the site. The Department will conduct follow-up inspections to insure compliance. | |
1940798 | 2010-11-02 | No Violations Noted | New sediment trap installed to control water going onto neighboring property. | |
1962046 | 2010-11-16 | No Violations Noted |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 188385.3 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 212807.44 | 182.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 293089.73 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 254686.7 | 181.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 25110.62 | 52.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-3 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2009-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | PRODUCED FLUID | 37.0 | Bbl | INJECTION DISPOSAL WELL | 34-031-27177 | ADAMS #1 (SWIW #10) - PREFERRED FLUIDS MGT LLC | COSHOCTON | OH |
2012-2 | PRODUCED FLUID | 52.0 | Bbl | INJECTION DISPOSAL WELL | 34-013-20609 | BUCKEYE UIC BARNESVILLE #1 (SWIW#2) - CNX GAS CO | BARNESVILLE | OH |
2012-2 | PRODUCED FLUID | 90.0 | Bbl | INJECTION DISPOSAL WELL | 34-121-23995 | HUNTER DISPOSAL - WARREN DRILLING CO #1 (SWIW #6) | DEXTER CITY | OH |
2012-2 | PRODUCED FLUID | 819.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2010-2 | PRODUCED FLUID | 893.64 | Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026913 | MCKEESPORT SEWAGE TREATMENT PLANT | MCKEESPORT | PA |
2011-1 | PRODUCED FLUID | 35.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0026824 | CLAIRTON MUNICIAPL AUTHORITY - SEWAGE PLANT | CLAIRTON | PA |
2011-1 | PRODUCED FLUID | 2491.0 | Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026913 | MCKEESPORT SEWAGE TREATMENT PLANT | MCKEESPORT | PA |
2011-1 | PRODUCED FLUID | 878.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE OF BRINE TO FRAC A WELL | |||
2011-2 | PRODUCED FLUID | 973.46 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE OF BRINE TO FRAC A WELL | |||
2012-1 | PRODUCED FLUID | 770.21 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |