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Difference between revisions of "37-115-20728"

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| Operator Name: [[CABOT OIL & GAS CORP|CABOT OIL & GAS CORP]]
 
| Operator Name: [[CABOT OIL & GAS CORP|CABOT OIL & GAS CORP]]
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| Well Pad ID: [[148519]]
 
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| Farm/Lease Name: R HESS 5
 
| Farm/Lease Name: R HESS 5

Revision as of 23:08, 13 June 2014

Well Details

Well ID: 42-115-20728
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County: Susquehanna
Municipality: Dimock Township
Operator Name: CABOT OIL & GAS CORP
Well Pad ID: 148519
Farm/Lease Name: R HESS 5
First Permit Date: 2011-11-18
Last Permit Date: 2011-11-18
Spud Date: 2012-02-06
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 41.759452
Longitude: -75.868772

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
2047097 2012-02-28 No Violations Noted H&P 290. At 2820' while drilling on air encountered @4000 units of gas. Initially killed well with mud. Tried drilling out on fluid, then lost circulation and continued to get gas. Set 2 - 500' cement plugs and capped well. Skidded over to Hess 2H well. Currently no pressure on 5H well. At this time no plans made to continue on this well.
2047100 2012-02-29 No Violations Noted Follow up on Well pressure on well. Well has been capped due to high pressure encountered while drilling on air at @ 2800'. Two cement plugs have been set to seal off gas. There are three gauges on the capped well. All three are showing no pressure at this time.
2065316 2012-05-01 No Violations Noted H&P 290. Tripping in hole now to resume drilling lateral. Had previously hit large gas due to fracture encountered at 2820'. At that time set two (2) 500' cement plugs and moved off hole to drill other wells on pad. Drilled offset of cement plugs to avoid fracture. Company Man indicated that some mud loss was observed at same depth (2820'), but no gas kick occurred this time mainly because this time drilling on fluid. TD proposed is @ 13,300'. 7" casing was set at 3317' with 44.1 bbls cement. FIT run @ 3317' at 1121 psi on 8.5 ppg = 15 ppg EMW. Drillers log on site and up to date.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 2164063.57 162.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 FRACING FLUID WASTE 6474.74 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-2 PRODUCED FLUID 3472.01 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-2 FRACING FLUID WASTE 1674.74 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NE001 SOMERSET REG WATER/SUSQ BENEFICIAL REUSE FAC SPRINGVILLE PA
2012-2 PRODUCED FLUID 59.36 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NE001 SOMERSET REG WATER/SUSQ BENEFICIAL REUSE FAC SPRINGVILLE PA
2012-2 BASIC SEDIMENT 33.93 Bbl LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH
2012-2 FLOWBACK FRACTURING SAND 7.73 Tons LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH
2012-2 FLOWBACK FRACTURING SAND 0.51 Tons LANDFILL 101534 WASTE MANAGEMENT, INC - LAUREL HIGHLANDS LANDFILL JOHNSTOWN PA
2012-2 FLOWBACK FRACTURING SAND 6.31 Tons LANDFILL 100081 WASTE MANAGEMENT, INC - SOUTHERN ALLEGHENIES DAVIDSVILLE PA
2012-1 DRILL CUTTINGS 555.58 Tons LANDFILL NY STATE #32S11 ALLIED WASTE SYSTEMS NIAGARA FALLS NY
2012-1 DRILLING FLUID WASTE 373.33 Bbl LANDFILL NY STATE #32S11 ALLIED WASTE SYSTEMS NIAGARA FALLS NY
2012-1 FLOWBACK FRACTURING SAND 16.21 Tons LANDFILL 100945 CUMBERLAND COUNTY LANDFILL NEWBURG PA
2012-1 FLOWBACK FRACTURING SAND 4.0 Tons LANDFILL 101571 MOSTOLLER LANDFILL SOMERSET PA
2012-1 DRILLING FLUID WASTE 371.25 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-1 FRACING FLUID WASTE 3212.01 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-1 DRILL CUTTINGS 904.23 Tons LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH
2012-1 DRILLING FLUID WASTE 785.04 Bbl LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH
2012-1 DRILLING FLUID WASTE 5.45 Bbl LANDFILL 101534 WASTE MANAGEMENT, INC - LAUREL HIGHLANDS LANDFILL JOHNSTOWN PA
2012-1 FLOWBACK FRACTURING SAND 8.81 Tons LANDFILL 101534 WASTE MANAGEMENT, INC - LAUREL HIGHLANDS LANDFILL JOHNSTOWN PA
2012-1 DRILLING FLUID WASTE 4.67 Bbl LANDFILL 100081 WASTE MANAGEMENT, INC - SOUTHERN ALLEGHENIES DAVIDSVILLE PA

References