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34-155-23390

Well Details

Well ID: 34-155-23390
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1991-01-29
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 41.3698334654
Longitude: -80.9110807903

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1033556962 2011-07-19 The well needs identification that includes:

Owner Emergency telephone number County Permit Number Lease Name Well Number

9-9-05(A)10
-2145785113 2004-04-01 Restoration approved .
1317235381 2011-09-28 A follow-up found the compliance notice resolved. A complete ID was on display at the tank battery.
1346334616 2011-07-19 FOLLOW UP TO NOV # -1033556962 The well needs identification that includes:

Owner Emergency telephone number County Permit Number Lease Name Well Number

1378397436 2013-09-05 My inspection found the well not in production. The tank battery and well were completely overrun by weeds. The proper identification sign was posted; however, the emergency contact phone number did not work. The tank battery was shared with permit number 2-1142. I researched out database and found no production reported since 2009. The phone number listed in our database did not belong to the Briswell Company. I found a new contact phone number and called Briswell Company at 330-759-8005. Briswell claimed the well was shut-in and they were considering on either plugging the well or selling the well to the landowner. I told the Briswell Company that a compliance notice would be issued for non-production. Also, I informed Briswell that the tank battery was overrun by weeds. I gave Briswell until 10/4/2013 to produce, file for plugging permit, or file for temporary inactive status. I took photos of the well site. NONE_
1378397436 2013-09-05 My inspection found the well not in production. The tank battery and well were completely overrun by weeds. The proper identification sign was posted; however, the emergency contact phone number did not work. The tank battery was shared with permit number 2-1142. I researched out database and found no production reported since 2009. The phone number listed in our database did not belong to the Briswell Company. I found a new contact phone number and called Briswell Company at 330-759-8005. Briswell claimed the well was shut-in and they were considering on either plugging the well or selling the well to the landowner. I told the Briswell Company that a compliance notice would be issued for non-production. Also, I informed Briswell that the tank battery was overrun by weeds. I gave Briswell until 10/4/2013 to produce, file for plugging permit, or file for temporary inactive status. I took photos of the well site. NONEC
1380894081 2013-10-04 My inspection found all of the weeds cut down in and around the tank battery. The tall grass was cut down from the tank battery to the pumping unit per my request. The dike meets containment requirements. The proper identification signs was posted on the production tank and the well. I spoke with Mr. Kondolean of Briswell at 330-759-8005. Mr. Kondolean the company was working on putting the well back into production; however, there was an issue with getting power to the pumping unit. I gave Briswell an extension to 11/18/2013 to place the well into production.
1759623309 2014-05-28 I was on location for a follow-up inspection in reference to compliance notice #1378397436. I found during my inspection that Briswell Co. had power run to the pumpjack. The weeds were all cut down in and around the dike. The proper identifications were posted on the production tank and well. I found no further violations.
99877780 2002-10-24 Meets requirements.