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34-007-24343

Well Details

Well ID: 34-007-24343
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2004-09-01
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 41.5579565331
Longitude: -80.8811569005

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-277768102 2004-09-01 Cappstar drilling co. rigging up drilling rig .
-340698356 2012-01-11 no violations .
-700928852 2004-09-14 Rig has moved off site . Drilling pits have closed .
1407198730 2014-07-23 My inspection of this well was in response to a house explosion at 4033 Montgomery Road. Upon arrival at the well location, I found the surface casing head below ground level. The company excavated around the well to expose the surface casing head. We found the annulus of the production casing sealed. We slightly opened the 2 valve to find there was pressure on the annulus of the production casing. I placed a pressure gauge on the 2 valve to find 80 psi. We then opened the valve, and the pressure dropped to 0 psi in 3 minutes. The tubing pressure was 145 psi and the production casing was 180 psi. I found no compliance issues with this well.
292969096 2006-04-11 no violations .