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Well ID: 34-007-24343 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2004-09-01 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 41.5579565331 | |
Longitude: -80.8811569005 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-277768102 | 2004-09-01 | Cappstar drilling co. rigging up drilling rig . | ||||
-340698356 | 2012-01-11 | no violations . | ||||
-700928852 | 2004-09-14 | Rig has moved off site . Drilling pits have closed . | ||||
1407198730 | 2014-07-23 | My inspection of this well was in response to a house explosion at 4033 Montgomery Road. Upon arrival at the well location, I found the surface casing head below ground level. The company excavated around the well to expose the surface casing head. We found the annulus of the production casing sealed. We slightly opened the 2 valve to find there was pressure on the annulus of the production casing. I placed a pressure gauge on the 2 valve to find 80 psi. We then opened the valve, and the pressure dropped to 0 psi in 3 minutes. The tubing pressure was 145 psi and the production casing was 180 psi. I found no compliance issues with this well. | ||||
292969096 | 2006-04-11 | no violations . |