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Well ID: 115-20594 | Loading map...
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County: Susquehanna | |
Municipality: Springville Township | |
Operator Name: CABOT OIL & GAS CORP | |
Farm/Lease Name: AUGUSTINE 3 | |
First Permit Date: 2011-06-17 | |
Last Permit Date: 2011-06-17 | |
Spud Date: 2011-08-01 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 4 | |
Latitude: 41.688636 | |
Longitude: -75.922086 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1990340 | 2011-07-22 | No Violations Noted | ||
2000375 | 2011-08-25 | No Violations Noted | Patterson 252. Company Man not available. 13 3/8" cemented with 460 sks with 25 bbl returns. Set at 585'. Floats held. Secondary containment in place and in good condition. | |
2005264 | 2011-09-21 | No Violations Noted | Follow up on status of well. Operator had taken excessive gas kick and have been in process of pluggin off gas so they can kick off and drill out. Drill pipe is free @3940'. Well is currently dead with 17.1 mud weight. Coil tubing unit ran out of diesel and uncoiled. At time of inspection trying to get tubing out of hole. Coil tubing unit on site to displace water in drill pipe with 17.1 mud. | |
2007054 | 2011-08-23 | Violation(s) Noted | 621318 | |
2007054 | 2011-08-23 | Violation(s) Noted | 621319 | |
2007193 | 2011-09-27 | No Violations Noted | Patterson 252. Have cement plug set. Top of plug at 3350'. Currently no gas present above plug. Bottom of pipe at 3935'. Have 16.6 wt mud in hole and are slowly reduing mud wt at .10 lb at a time ciculating 5 bottoms up each interval. | |
2007204 | 2011-08-29 | Violation(s) Noted | 621333 | |
2007204 | 2011-08-29 | Violation(s) Noted | 621334 | |
2007235 | 2011-08-25 | No Violations Noted | ||
2009267 | 2011-10-03 | No Violations Noted | Patterson 252. Flaring at time of inspection. Currently circulating 4 bottoms up at .10 ppg mud weight intervals. Currently at 13.7 ppg. Goal is to bring mud wt down to water weight equivalent while working gas up out of the hole. Drill pipe bottom is at 3300' (50 ' off bottom). Will continue to circulate for several days. | |
2012667 | 2011-10-19 | No Violations Noted | DEP on site 11:30. Patterson 252. Currently at 11.8 mud wt. Previously weighted down to water wt.and still had minimal amount of gas. At time of inspection rig broke down. Will be going back in hole to tag TOC. Eventually will be running 7" casing to fracture zone @5600' and produce through 7". DEP off site at 12:25. | |
2119423 | 2012-11-21 | No Violations Noted |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 4177.68 | 16.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | FRACING FLUID WASTE | 7345.37 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-2 | PRODUCED FLUID | 79.6 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-2 | FRACING FLUID WASTE | 1986.67 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NE001 | SOMERSET REG WATER/SUSQ BENEFICIAL REUSE FAC | SPRINGVILLE | PA |
2012-2 | BASIC SEDIMENT | 0.74 | Bbl | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-2 | DRILLING FLUID WASTE | 717.17 | Bbl | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-2 | FLOWBACK FRACTURING SAND | 12.16 | Tons | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-2 | DRILL CUTTINGS | 124.76 | Tons | LANDFILL | 301626 | WHITE PINES LANDFILL | MILLVILLE | PA |
2011-2 | DRILL CUTTINGS | 194.32 | Tons | LANDFILL | 101247 | KEYSTONE SANITARY LANDFILL | DUNMORE | PA |
2011-2 | DRILL CUTTINGS | 7.47 | Tons | LANDFILL | 101534 | LAUREL HIGHLANDS LANDFILL | JOHNSTOWN | PA |
2011-2 | DRILLING FLUID WASTE | 4722.57 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE OF BRINE TO FRAC A WELL | |||
2011-2 | DRILL CUTTINGS | 3320.09 | Tons | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2011-2 | DRILL CUTTINGS | 5.69 | Tons | LANDFILL | 100081 | WASTE MANAGEMENT, INC - SOUTHERN ALLEGHENIES | DAVIDSVILLE | PA |