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34-121-21562

Well Details

Well ID: 34-121-21562
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County: Noble
Municipality:
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1972-09-19
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.8282474
Longitude: -81.51214508

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 0.0 0.0
1986-0 0.0 0.0
1987-0 0.0 0.0
1988-0 0.0 0.0
1989-0 0.0 0.0
1990-0 11528.0 0.0
1991-0 14142.0 11.0
1992-0 10026.0 0.0
1993-0 8185.0 0.0
1994-0 7000.0 0.0
1995-0 5876.0 0.0
1996-0 5614.0 0.0
1997-0 5158.0 0.0
1998-0 3249.0 0.0
1999-0 5048.0 0.0
2000-0 3951.0 0.0
2001-0 2322.0 0.0
2002-0 2888.0 0.0
2003-0 2847.0 0.0
2004-0 3177.0 16.0
2005-0 2980.0 0.0
2006-0 1262.0 0.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1064921763 2003-09-29 Anonymous complaint stated chronically leaking gas well.Upon inspecting well site and tank pad found no leaks at wellhead or in flowlinebut found production tank to have hole in side of tank.Called well owner and suggested they remove bad tank from dike a
-1269097768 2012-06-18 Inspection of the well head found the following equipment -8.626 surface casing -4.5 production casing & 1.5 tubing - plunger lift well with the commercial valves closed and a domestic hook up present and the valve open . A 210 barrel tank -separator and gas meter with no current sales chart are present in an established dike with proper well identification .Inspector will note, producing wells in immediate area are believed to be shut in due to property dispute at the compressor site.
1379610267 2013-09-19 My inspection today finds the well is equipped with 4.5 casing, 1.5 tubing with a plunger lift system. The commercial valves are shut; however the well appears to be produced for domestic proposes. I can hear gas flowing through the domestic tap. There is no vegetation in a three foot circle around the well. I did not hear any subsurface leak. The tank battery consists of one 210 bbl tank, a separator, and a meter. The chart on the meter shows a date of 5-1-07 from a UCP meter test.
411253206 2003-10-07 anonomus complaint upop inspecting well site for second time could not find any leaks in line ,the bad tank within dike is too be replaced by 11-1-03

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.