X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-169-20775

Well Details

Well ID: 34-169-20775
Loading map...
County: Wayne
Municipality:
Operator Name: S & H WATER SERVICE
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1958-07-01
Unconventional: No
Configuration: Vertical
Well Status: Active Injection
Violations: 0
Latitude: 40.67044074
Longitude: -81.93779455

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 0.0 327.0
1990-0 0.0 121.0
1991-0 0.0 60.0
1992-0 0.0 61.0
1994-0 0.0 0.0
1995-0 0.0 91.0
1996-0 0.0 155.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1009104168 2008-04-21 Compliance Notice
-1009104168 2008-04-21 Compliance Notice
-1009104168 2008-04-21 Field Visit or Inspection
-1009104168 2008-04-21 Compliance Notice
-1009104168 2008-04-21 Compliance Notice
-1009104168 2008-04-21 Field Visit or Inspection
-1009104168 2008-04-21 Field Visit or Inspection
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
-1009104168 2008-04-21
10175955 2002-01-18
-1025434100 2014-06-27 An inspection of the well and injection facility found no violations.
1069081117 2003-11-06
1077206924 2004-02-19 Injection Pressure 585- Annulus Pressure -0
1085595618 2005-06-01 Clean up complete and injection pressure down.
1093881886 2004-08-30 Injection pressure-650 Annulus pressure-0
-1107702886 2004-01-20 Injection pressure675 annulus pressure 20
-1124969501 2008-06-06 Arrive for test and found that packer and tubing had been left in the well and that they are now fishing packer out.Test was scheduled for 7:45 am I waited to 9:15 before anybody arrived.It was then I found out that tubing and packer was in the well and that they were out getting fishing license.I advised of the limits for Ohio and they all had to have a license to go fishing.
1129308059 2006-09-06
-116214861 2003-01-07
1199294473 2007-11-28
1210i2257178 2002-03-27 Snow cover. Well is operating. Need 1/4 tap at well head annulus. threads are bad unable to check pressures.) Id s need remarked and posted at the well and the tank battery. Accompanied by Tom Tomastik, and Dave Hodges.
-1212763928 2008-06-09 Witness rebuilt Halliburton R4 Packer go in hole with no tailpipe below packer.
1230096802 2012-06-29 I am checking to see if the needle valve has been installed so that I can check the injection and annulus pressure. I found that there was a small leak on the tubing and no needle valve has been installed. Contact Gary and advise of leak and needle valve repair.
-1230804845 2007-03-07
1239i40
1243395965 2010-06-07
1255801080 2011-04-25
-1283577890 2009-05-26
1317732369 2011-09-08
-1331741246 2014-12-09 The injection well and surface facility were inspected. A new needle valve was installed on the casing. As requested, the well tender pressurized the tubing/casing annulus. The pump was shut down for maintenance at the time. There were no violations found.
1347298074a 2012-09-19
1349888743 2009-08-17
1369227212 2013-03-28 FOLLOW UP TO NOV # 1365013865 My inspection of the well and surface facility found the following: The 1/4 inch threads on the annulus were worn and corroded, preventing access with a gauge. There was an erosion gully at the well road access.

A 1/4 inch, female, threaded fitting with a stop valve must be installed on the tubing/casing annulus. Ensure all valves at the well head are in working order. Repair the lease road access, in order to prevent further erosion.

-1379232865 2010-07-27
-1399464943 2005-08-29 Met Gary on site and went over well operation .
1412165485 2014-09-29 A valve, necessary to monitor the annular pressure, was stuck shut. A company representative was instructed to repair or replace the valve and put a minimum pressure of 200 psi. on the tubing/casing annulus.
1429028201 2015-04-10 The rig ran 94 joints of 2-3/8 EUE tubing to 2914'. Petroset displaced 34 bbls of fresh water with 3.5 gallons of Halliburton Ahhib into the annulus. The packer was then set in tension with 12,000 over string weight. The annulus was pressured up to 730 psig for 15 minutes with only a 10 psig loss in those 15 minutes. The test Passed.
1522819773 2005-10-20 FAILURE TO SUBMIT ANNUAL SALTWATER INJECTION WELL REPORTS FOR 2003 AND 2004
-1536865489 2010-06-23
-1546035982 2008-09-04
1564927060 2009-04-13 Well was operating with such a bounce that pressure appeared to be over .After using needle valve to close in found that it was at the limit but not over. Had a lot of air or something in the pump .
-156980288 2006-03-20
15821747 2005-08-15
-1600364272 2005-02-09
1618733403 2007-09-24
-1624237338 2012-09-10 My inspection of the well and injection facility found no violations. The pump was operating.
-163864854 2008-01-23
-1643053294 2014-03-06 Inspection revealed no apparent problems at time of inspection. Pump was not in operation.
-164372721 2006-01-19 The wellhead has had some leaks repaired and may leak again soon due to the repair.The well needs to be monitored more frequently than it is now .It should be every day and that does not appear to be the case.
1678354744 2010-11-16
-1697168157 2006-03-10
-1718361979 2005-12-28
1744120854 2013-07-24 All infractions in NOV 1365013865 have been corrected. NOV is resolved at this time.
-1770899263 2008-09-29
1775453192 2011-09-27
1775678414 2007-10-09
17876033 2002-03-19 Well is in operation and there are two tanks that are on site that are not part of the facility that need diked or removed.
1789314307 2009-03-26 There has been a spill below pumphouse.The pump leaked and now there is a line connected to unloading pad .This is a bypass but has enough brine mixed in with it that it has a kill area below pump area.Contact Gary and advise on bypass ,advise remove ASAP. Remain on site until pumper came and disconnected it.
1815122055 2008-05-27 Found well injection and annulus pressure to be the same.Contact Gary and advise.
-1848313088 2010-01-25 Check new installed injection line again for leaks and found none.
1886221272 2007-03-27
-1932655070 2009-03-02 Valves on annulus frozen and could not be checked .
-1940855946 2008-12-10
-197230924 2007-11-08
-2025229678 2009-11-05 The injection line has been replaced and they did not call for test of line.Walk line and there are no leaks .
2033705877 2005-04-26 Found burn barrels that are full of burned filters.The barrels are full and have running over and have caused a kill area aroung them.Issue NOV to Gary and he said that it would be cleaned up right away.Also advise that they are running up to the end of their pressure and it is going over after it shuts down.Advise Gary to fix the stops on his upper pressure switch.
-2036454604 2007-08-13
-206270080 2006-08-08 Arrived as the pumper was working on the pressure switch and found that well had been at the pressure limit .Chart shows that it was over and I advised pumper to repair pressure switch or replace it to maintain pressure below limit .
-2070340867 2007-09-24
-2099100920 2014-10-07 Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on February 15th for 2008, 2009, 2010, 2011, 2012, and 2013.
-2114112132 2006-12-01
2138953846 2003-07-02
2142697244 2008-06-03 Che.ck on rig and found that well is still flowing.Try and schedule for later today .
-224600966 2008-02-11
-233802391 2007-04-26
24078888 2002-08-19 Identification has been posted and fitting has been replaced. Cloudy 80 degrees. NOV in compliance.
27076088 2002-05-16 Wellsite does not have proper identification. Also advise on taps for both the injection and the annulus so that monitoring can continue.
271357933 2008-06-04 Well is still flowing back and is scheduled for test later today.Return later and found well is still flowing and is now scheduled for testing on Thursday.
27376091 2002-05-16 Met pumper on site and issue nov for Broken id. The plate is there but is broken into two pieces. Also issued nov for valve repair and install 1/4 inch access taps.
-277685507 2008-11-13
28576103 2002-06-05 Arrive to witness packer and bottom hole assembly go in hole. Buren well servoce ran a Halliburton R-4 packer in with no tailpipe below. Ran packer in on same 2 3/8 tubing string that was in in the hole . Ran packer to 2939 ft. pumped 40 bbl of Halliburto
32029795 2013-09-26 My inspection found the well in compliance. A 1/4 inch valve was installed on the tubing/casing annulus.
-324047963 2014-06-26 Well was not in operation at time of inspection. Due to exceedingly wet fields,unable to access well head. Tank battery and unload pad need some clean up; otherwise there were no apparent problems.
-327959587 2015-04-09 Moved on and rigged up and unjayed the R-4 packer. Waited until the element loosened up and pulled the tubing. No holes were fould in the tubing. The top joint will be replaced and the tubing run back in the morning.
340496227 2009-09-03
378293990 2013-07-22 All violations noted in NOV 1365013865 have been corrected. NOV is resolved at this time.
4075884
438788747 2008-03-25
-450028388 2007-01-24
-451076253 2006-11-15 Met Gary on site and went over clean up on other site .
452082611 2007-06-04
-46470548 2006-10-10
-471955030 2011-06-06 New 2 3/8 tubing line from pump to well site. Should have called to test line before using. Check line for leaks and found none. It is above ground, so easy to check for leaks.
48176228 2002-11-05 Found well pressure very close to each other and felt a bleed down test should be run to be sure pressure has not equalized .Contact Gary and advise of possible problem .Set test up for next day toward afternoon.
-494799217 2004-10-19
52380278 2005-05-12 Check on cleanup and pressure.Found clean up done and pressure under the limit.
537757897 2008-06-10 Maran Service rig ran 2 3/8 tubing in to 2932 ft. and Omega pumped 50 bbls freshwater and 4 gallons of Halliburton Anhib.Pressure test at 925 psi and test passed with no leak off at all.
543391434 2012-01-18 The pumphouse has been locked. The wellsite has been graded and trash removed. The annulus valve is frozen.
547489003 2013-05-09 Repairs have been made to the lease road. The required 1/4 inch fitting was not installed on the annulus. I was unable to gauge the annular pressure.
-552422984 2006-05-08 Met Gary on site to go over new well info .
-571432929 2008-06-18
-646805259 2008-07-22
653174103 2010-09-28
675858 2001-05-08
-688641007 2015-03-31 An inspection found excessive corrosion of the tubing and a section of injection line. The annular pressure was not gauged, because the two inch valve on the casing was split. A company representative, Joe Carter, was notified of the issues. The well owner was instructed to replace the tubing, valve, and the section of injection line.
690186079 2004-04-12 Injection pressure---650 Annulus pressure--0
-702519959 2013-11-14 On location today with Insp. Ochs to check status of well. Other than a few sealed bags of litter, there are no apparent problems at this time. Injection pump was in operation but the pump house was locked.
-73970647 2005-10-13
741460211 2008-12-15
745207161 2010-04-01 The new injection line appears to be doing well and there are no leaks.
766166765 2005-02-10 Return to site and found vaults full on the unloading pad and below the pumphouse.Had trucks on site pump out vaults and advise on Wyles filter burning .w/o Gary to arrive to go over info on NOV.
-767677548 2010-11-01
802080891 2011-01-03
804251703 2005-10-13
-815817510 2002-11-07 Test annulus for 15 minutes and after pressure had reached 675 on tubing the annulus remained at 100 psi.
-817440693 2003-04-15 Found small drip type leaks around 3 inch valve on wellhead and advise Gary that they need to be repaired or replace valve . Collect photos for Columbus.
82246278 2012-05-21 Contact operator and spoke to Gary. Advised him to replace the 2 inch bullplug and needle valve. The needle valve to install my gauge has been removed.
888345680 2008-01-14
-889885365 2007-09-11
-892511554 2008-06-02 Check on Maran Service rig and found that they are digging pits to flow back into.Well has not slowed down so that they can pull tubing and packer.Most likely will be Tuesday before tubing starts out of hole.
-931147792 2003-09-11 Found well over pressure and contacted Gary and advised on over pressure and he said he would fix the problem A.S.A.P.
-939176554 2011-03-01 Check well today with new Inspector Murphy.
PL1290 Preliminary Restoration done information from Data Point
UIC1079 1991-03-12 1509.03 RULES & REGULATIONS
UIC1080 1991-03-12 1501:9-3-04 PREVENTION OF CONTAM
UIC1103 1991-03-28 1509.03 PERMIT
UIC1517 1994-07-14 1509.22 (A) (2) STORAGE & DISPOSAL
UIC1518 1994-07-14 1501: 9-3-04 PREVENT CONTAMINATE
UIC1519 1994-07-14 1509.072 RESTORATION
UIC436 1987-12-03 1509.03
UIC547 1988-06-01 1509.072 (A)
UIC548 1988-06-01 1509.22 (A)(2)
UIC549 1988-06-01 1501:9-3-04(A)
UIC760 1989-08-30 1509.03 Conditions of permit
UIC873 1990-04-10 1509.03 RULES & REGULATION
UIC899 1990-04-18 1509.226 SURFACE APPLICATION

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.