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34-103-25012

Well Details

Well ID: 34-103-25012
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County: Medina
Municipality:
Operator Name: BLEACH TECH LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2007-09-17
Unconventional: No
Configuration: Vertical
Well Status: Active Injection
Violations: 0
Latitude: 41.02944439
Longitude: -81.98883267

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1029019195 2007-09-20 J.D.Drilling is at 350 ft on 12 1/4 hole.
1124937055 2007-09-22 J.D.Drilling set 612 ft. 8 5/8 casing c/w 340 sks - Petroset - Rich
-1172526615 2010-06-08 Priliminary restoration has been passed but service rig has been back so some restoration work in needed. Service rig is scheduled back again around the 4 th of July so after that .
1199279956 2007-10-03 Log well after J.D.Drilling laid down drill string . Then could not run 41/2 inch casing because it was too long for the rig to run.J.D is to bring out another rig to run casing.
1331830736 2012-02-16 Davis Well Service is working on this well today. The tubing needs to be set deeper since the roof collapse ripped off at least two of the bottom joints of tubing.
-1339537583 2012-10-03 On location to conduct a Water-Brine Interface Mechanical Integrity test.
-1340160076 2007-11-29 Check well and found pits closed and area graded.
-1366824042 2007-09-21 Called and scheduled job for 10 and during trip to site job was cancelled .
1422158432 2007-09-21 Travel to site for cement job and found on route that it is cancelled for today.
1564998696 2007-11-07 Met operator on site today and placed 5 sacks dry cement on the backside of 8 inch to firm casing up.
1666927655 2012-02-17 I checked on the Davis service rig and found that they are running tubing back in the hole. They should be able to get to same depth as before the roof collapse, or below.
1711474922 2007-09-19 J.D.Drilling is at 250 ft. on 12 1/4 surface hole.
1743497695 2012-04-04 I was on site today to witness the attempt to run a downhole camera in this well, after the tubing had been pulled. The tubing was cut off from a roof collapse this same day. They were unable to get camera down this well either.
1802046586 2007-09-27 J.D.Drilling is at 1500 ft. dusting on 7 7/8 hole.
-1945902250 2008-03-21 Well is in operation. Equipped with tubing and flow lines. GPS location.
-2018253214 2008-09-10 Needs more vegetaion established on entire well site.Met with field man and advise more vegetation.
2122494012 I checked this well to see if the tubing had been re-installed. I found the tubing back in the well and pressure on the casing.
2134337292 2007-10-01 J.D.Drilling is at 2200 ft. on 7 7/8 hole.Should finish up on Weds.
282857639 2009-06-16 Pull tubing today and replace with another string.Well in connected to the # 4
-305615049 2007-10-10 Arrive today to inspect well and found that rig is done and moved.Pit level and liner good.
342791429 2010-05-03 Check wells and found them in operation.
35282265 2008-07-17 Arrive today and found that Glenn Davis is pulling 2 3/8 tubing out and running in a new string .The tubing had a hole in it and found several bad joints so they are running in with a new string.
370733793 2007-09-22 Arrive today to set surface casing .J.D.Drilling set 612 ft. of 8 5.8 casing c/w 340 sks Petroset - Paul -Rich
396198285 2007-09-17 Moving rig in today and should start drilling.Pit level and liner are good.
422561536 2007-09-27 J.D.Drilling is at 1500 ft. dusting on 7 7/8 hole.
467786997 2008-07-18 Return to find that tubing is back in well and that they are back in operation.
-679334849 2007-09-19 J.D.Drilling is at 250 on 12 1/4 surface hole.
-750950070 2007-09-17 J.D.Drilling is movin rig in today to start on next well .Pit level and liners ok
752222468 2007-10-11 Arrive today for M.I.T. test and also cement bond log.Test well to 500 P.S.I. For 15 minutes and test passed.Bond log looked good.
-824728567 2007-09-21 J.D.Drilling is at 350 ft. on 12 1/4 surface hole and should be ready to set surface on Friday.
-924985950 2007-10-08 J.D.Drilling set 2438 ft. of 4 inch casing c/w 600 sks.Petroset
-998397499 2007-10-05 Arrive to run casing again and J.D.Drilling could not get casing to bottom. After circulating still could not get casing to bottom.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.