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37-063-27120

Well Details

Well ID: 37-063-27120
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Operator Name: EXCO RESOURCES PA LLC
First Permit Date: 1982-07-12
Last Permit Date: 1982-07-12
Spud Date: 1983-02-09
Unconventional: No
Horizontal: No
Violations: 1
Latitude: 40.630451
Longitude: -79.048064

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 875.0 365.0 0.0 0.0 0.0 0.0
2012-0 899.0 366.0 0.0 0.0 0.0 0.0
2011-0 449.0 365.0 0.0 0.0 0.0 0.0
2010-0 330.0 365.0 0.0 0.0 0.0 0.0
2009-0 748.0 365.0 0.0 0.0 0.0 0.0
2008-0 611.0 365.0 0.0 0.0 0.0 0.0
2007-0 0.0 0.0 0.0 0.0 0.0 0.0
2006-0 0.0 0.0 0.0 0.0 0.0 0.0
2005-0 0.0 365.0 0.0 0.0 0.0 0.0
2004-0 0.0 365.0 0.0 0.0 0.0 365.0
2003-0 226.0 365.0 0.0 0.0 0.0 0.0
2002-0 0.0 365.0 0.0 0.0 0.0 0.0
2001-0 0.0 0.0 0.0 0.0 0.0 0.0
2000-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-0 PRODUCED FLUID 70.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY JOSEPHINE PA
2008-0 BRINE 160.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT PA BRINE TRT - JOSEPHINE PLT -INDIANA CO
2009-0 BRINE 310.0 Bbl INJECTION DISPOSAL WELL IRVIN A SALT WATER DISPOSAL
2009-0 BRINE 310.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT PA BRINE TRT - JOSEPHINE PLT -INDIANA CO
2010-0 PRODUCED FLUID 64.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095443 HART RESOURCE TECHNOLOGIES, INC. - CREEKSIDE CREEKSIDE PA
2010-0 PRODUCED FLUID 80.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAS2D205BCLE IRVIN A SALTWATER DISPOSAL PA
2012-0 PRODUCED FLUID 70.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY JOSEPHINE PA
2013-0 PRODUCED FLUID 2.0 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273 FLUID RECOVERY SERVICE JOSEPHINE FACILITY JOSEPHINE PA

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1806311 2009-06-01 No Violations Noted stray gas complaint - gas bubbling @ shoreline & in Two Lick Lake/equipped & in production - annulus open - no visible gas/pipe line to be shut-in & tested/gas samples collected from well & shorline by Fred Baldassare.
1806312 2009-06-02 No Violations Noted pipeline shut-in @ 11:30 with 85psi - will remain shut-in for 24hrs/gas still bubbling @ previous spots
1806327 2009-06-09 No Violations Noted pipeline test 24hrs - no pressure loss - remained 84psi/gas bubbling continues in same spots
1807441 2009-06-16 No Violations Noted 48hr pipeline pressure test set-up/pipeline shut-in @ 90psi
1807447 2009-06-18 No Violations Noted Pressure test complete - 90psi held for 48hrs
1809213 2009-06-24 No Violations Noted check status of stray gas - gas continues to bubble @ Two Lick Lake shoreline & approx. 100yds out in the lake.
1810040 2009-06-08 No Violations Noted check'd pipeline pressure test - held @ 84psi.
1811741 2009-07-10 Violation(s) Noted 566771
1825855 2009-08-26 No Violations Noted equipped - producing/temp E&S ok/tag ok/conditions unchanged - intent to plug submitted
1831783 2009-09-22 No Violations Noted equipped - operator scheduling to plug due to stray gas in area/E&S ok/tank&tag ok

References