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Well ID: 37-047-21311 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Highland Township | |
Operator Name: SENECA RESOURCES CO LLC | |
Well Pad ID: | |
Farm/Lease Name: ALLEGHENY NATL FOREST 98P | |
License Status: INACTIVE | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.469650 | |
Longitude: -78.872274 |
Date | Event |
---|---|
1983-06-01 | Drilling Completion |
1983-11-17 | REWORKED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | NATL FUEL GAS SUPPLY CORP | 2004.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1992 | NATL FUEL GAS SUPPLY CORP | 1697.00 | 366 | 0.00 | 0 | 0.00 | 0 |
1993 | NATL FUEL GAS SUPPLY CORP | 1716.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1994 | NATL FUEL GAS SUPPLY CORP | 1883.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1995 | SENECA RESOURCES CO LLC | 2336.65 | 360 | 0.00 | 0 | 0.00 | 0 |
1996 | SENECA RESOURCES CO LLC | 1623 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | SENECA RESOURCES CO LLC | 1791 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | SENECA RESOURCES CO LLC | 1180 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | SENECA RESOURCES CO LLC | 140 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2001 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2002 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2490796 | Primary Facility | 2016-04-27 | Routine/Complete Inspection | No Violations Noted | |
2494218 | Primary Facility | 2016-06-14 | Routine/Complete Inspection | No Violations Noted | |
2508247 | Primary Facility | 2016-07-28 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2510693 | Primary Facility | 2016-08-12 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2545832 | Primary Facility | 2016-12-16 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2829827 | Primary Facility | 2019-01-22 | Routine/Complete Inspection | No Violations Noted | This plugged well had gas coming into it at around 50' below surface through the water table since it was plugged a few years ago. Today I checked the well and got a zero reading on my meter and I couldn't hear any bubbling down hole only water running in. The water level is high at this time but this is the first time I have gotten a zero reading in the years of checking it. I notified Seneca resources of my findings and will continue to monitor the well for any gas and ask Seneca to monitor it too. |
2849257 | Primary Facility | 2019-03-06 | Routine/Complete Inspection | No Violations Noted | This plugged well had gas coming into it at around 50' below surface through the water table since it was plugged a few years ago. There has been other plugging in the area and I was periodically checking the well for gas. On 1/22/19 I found the well no longer was leaking and I checked the well on 1/25/19, 2/1/19, 2/14/19, 2/22/19 and today 3/6/19 and have gotten a zero reading each time. Before you could hear the gas bubbling from across the location and I was getting 100% methane readings and now there is no bubbling and only water trickling into the well. The water level in the well is about 50' at this time.
I spoke with Dave Way from Seneca Resources and gave them permission to go ahead and top hole the well by filling it with pea gravel. |
370124 | Primary Facility | 1991-09-25 | Routine/Complete Inspection | No Violations Noted | |
372594 | Primary Facility | 1992-10-14 | Routine/Complete Inspection | No Violations Noted |
For data sources see[6]