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34-019-22220

Well Details

Well ID: 34-019-22220
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-460084422 2012-12-07 I was on site to witness the cementing of the 20" conductor casing. Inspection revealed that Precision Rathole has drilled a 26" hole to 36' and a 24" hole from 36' to 120'. They ran 109' of 94 pound per foot 20" casing. Allied Cementing Company cemented the casing with 171 sacks of Class "A" cement (2% CaCl and .5 pound per sack floseal). The cement had a density of 15.6 pound per gallon and and a yield of 1.18 cubic feet per sack. There was good circulation throughout the job and there was approximately 10 barrels of cement circulated to surface. I walked the perimeter of the well site and found no erosion/sedimentation on any of the slopes of the well pad. No violations were noted at this time.