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Well ID: 34-067-20221 | Loading map...
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County: Harrison | |
Municipality: | |
Operator Name: CHEVRON APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1975-05-05 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 40.19678174 | |
Longitude: -81.29943779 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 0.0 | 0.0 | ||||
1985-0 | 0.0 | 0.0 | ||||
1987-0 | 11558.0 | 0.0 | ||||
1988-0 | 6501.0 | 0.0 | ||||
1989-0 | 4585.0 | 89.0 | ||||
1990-0 | 5324.0 | 0.0 | ||||
1991-0 | 5288.0 | 82.0 | ||||
1993-0 | 4445.0 | 0.0 | ||||
1994-0 | 2887.0 | 0.0 | ||||
1995-0 | 0.0 | 0.0 | ||||
1996-0 | 0.0 | 0.0 | ||||
1997-0 | 0.0 | 0.0 | ||||
1998-0 | 0.0 | 0.0 | ||||
1999-0 | 0.0 | 0.0 | ||||
2000-0 | 0.0 | 0.0 | ||||
2001-0 | 0.0 | 0.0 | ||||
2002-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 118.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1110382263 | 2005-03-07 | Inspection revealed that the well is an idle well ; incapable of production . The separator has been unhooked and the the wellhead is shut in (valves are rusted ) . Production reports submitted by the operator to Columbus indicates that there hasn't been any production reported since 1995 . The operator needs to plug or produce the well . Remedial action must be completed by April 11th, 2005 . | Compliance Notice | |||
1110382263 | 2005-03-07 | Inspection revealed that the well is an idle well ; incapable of production . The separator has been unhooked and the the wellhead is shut in (valves are rusted ) . Production reports submitted by the operator to Columbus indicates that there hasn't been any production reported since 1995 . The operator needs to plug or produce the well . Remedial action must be completed by April 11th, 2005 . | Compliance Notice | |||
1110382263 | 2005-03-07 | Inspection revealed that the well is an idle well ; incapable of production . The separator has been unhooked and the the wellhead is shut in (valves are rusted ) . Production reports submitted by the operator to Columbus indicates that there hasn't been any production reported since 1995 . The operator needs to plug or produce the well . Remedial action must be completed by April 11th, 2005 . | Compliance Notice | |||
1141705939 | 2006-02-24 | Jim Hershman complaint of idle well and occasional H2S gas odor . Inspection of the well revealed that the well is idle . The valves on the wellhead are all closed and rusted . Parts of the separator is missing and the gas sales line is unhooked . I am issuing a written NOV to Atlas America to plug or produce the well . Note: There is a faint H2S gas odor at the wellhead at this time . I didn't have my gas detector with me to check the H2S gas levels . | ||||
1145988249 | 2006-04-19 | On site to witness the bottom hole plug ( Clinton Plug ) . Formation cementing pumped a 25 sk plug thru tubing to plug from 5644 to 5344 . H2S gas odor while they were pumping the plug . Gary Haught advised that they were going to rip the 4 1/2 casing and pull the casing because there is a hole in the casing . They are going to run tubing back into the well to finish plugging the well . Should be ready on Monday morning to finish plugging the well . | ||||
-1228800905 | 2006-04-18 | Inspection revealed that Cardinal Well Services has fished the 1 1/2 tubing out of the well and are running the 2 3/8 upset tubing back into the well to spot the bottom hole plug tomorrow morning . | ||||
1500062950 | 2006-04-21 | On site today to finish plugging the well . Pumped the Clinton plug on 04/19/2006 . Pumped the lime plug , bottom 8 5/8 plug , berea plug , and the surface plug . Well has plugged and abandoned . This well is associated with the Jim Hershman complaint . Case can be resolved at this time . | ||||
-1685794241 | 2013-09-16 | On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B. | ||||
1875421302 | 2006-04-18 | Inspection revealed that Cardinal Well Services is running a fishing tool back into the well with tubing ; trying to fish out the 1 1/2 tubing that H2S gas rotted of at app. 2785'. They got ahold of the tubing with the fishing tool and started coming out of the hole . I advised that I would return to the site later today to check on the progress of the fishing job. | ||||
667582127 | 2006-04-13 | Inspection revealed that the well is still idle . Talked with Terry Whitehair and he advised that they are applying for the plugging permit and that they need a couple of more weeks to get the well plugged . I advised that they can have an extension until 04/28/06 . |
For data sources see[2]