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34-119-26178

Well Details

Well ID: 34-119-26178
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County: Muskingum
Municipality:
Operator Name: STONEBRIDGE OPERATING CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-11-17
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.85438207
Longitude: -82.14194468

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 5862.0 1973.0
1985-0 3414.0 945.0
1986-0 4242.0 945.0
1987-0 1879.0 463.0
1988-0 1665.0 350.0
1989-0 1015.0 260.0
1990-0 1131.0 202.0
1991-0 1613.0 0.0
1993-0 1376.0 77.0
1994-0 921.0 98.0
1995-0 528.0 0.0
1996-0 870.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 56.0
2005-0 0.0 28.0
2006-0 0.0 0.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 33.0 0.0
2010-0 206.0 0.0
2011-0 356.0 1.0
2012-0 328.0 3.0
2013-0 70.0 7.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1260217497 2009-12-07 No gas sales. Looks like well is being or has pumped recently. Contacted the pumper who said the well was being pumped but now has a hole in the flowline. Roustabouts to fix it in the near future.
-1296314297 2009-08-11 FOLLOW UP TO NOV # -558646870 Not producing. No production reported for two years
1317835135 2011-10-04 On day of inspection well and tank site passed inspection. No violations noted.
1337109326 2012-05-15 On day of inspection well is supplied with a artificial lift system. There is no pressure on well and chart Graph is not being used. Id is in place. Well is not producing. Well is capable
1344560093 2012-08-09 I met with pumper Keith Kreagor on the well. The well is was issued a Compliance Notice due to not capable. There is an Artificial lift system on well. There is also two 100 barrel tanks. The well has been installed with a new logic control that starts electric motor on the artificial lift for 10 minutes every 5 hrs. The lines that flow to the tanks are open and the separator is bypassed. Compliance Notice is resolved on day of 8-9-12 by Patrick Shreve.
-1542566360 2012-04-16 On the day of my inspection I found the well to have been plugged, the production equipment has been removed, the pit has been back filled, the well location has been reclaimed, the roadway has been restored, there is good vegetation and erosion control.
1627265325 2009-09-01 Not producing.
-1805174785 2007-03-14 Well is not producing. Zero on meter has been adjusted to show production. No gas is being sold and the unit is not running. No royalties paid. No sales
1826810957 2006-09-06 Producing
-1954142470 2007-08-10 Oil spill in sided dike has seeped thruough dike
2146997954 2005-12-14 AD not in use. Well is not producing.
322455663 2006-12-20 Well is on line.
-558646870 2009-08-11 Not producing. No production reported for two years
705516767 2007-03-29 No gas sales not sure if pumping or not.
748023331 2012-10-12 Statis check
PL8599 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.