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34-153-22968

Well Details

Well ID: 34-153-22968
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2006-08-30
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 41.0179401791
Longitude: -81.5581874407

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1053097687 2006-09-06 Status check inspection found no violations. Union should finish the 9-7/8" hole in the next few days.
-1115146998 2011-10-11 This inspection was completed as part of the required five year mechanical integrity test (MIT). The test well is the 7" production casing in Akron #75. The reference well was the 7" casing in Akron #74 (PN-2967). The test began at 07:00 am and was concluded at 3:00 pm on 10/11/2011. The first pressure difference between the test well and the reference well was 424.071 psi. The final pressure difference between the test well and the reference well, eight hours later was 424.069 psi. Based on the pressure change from start to finish, the Akron 75 well easily passes this MIT.
-1293828886 2013-06-24 The well was properly identified. My inspection was accompanied by Andrew Adgate.
-1478332437 2006-09-12 The MIT was successfully completed on the 7" production casing. The initial shut in pressure was 560 psi with no change after 5, 10 and 15 minute intervals.
-1871638510 2009-06-18 Columbus requested an annual inspection of the solution mining wells. This inspection found no violations at this time.
-399983951 2008-12-31 Annual status check inspection found no violations at this time.
1089762204 2007-07-25 Preliminary restoration is approved.
1159994592 2006-09-27 The drilling rig has moved off and the site has been rough graded. The small cementing pit has also been closed. No violations at this time.
1733966972 2007-05-16 Preliminary restoration is due this month. The site still needs to be finish graded, topsoil spread, seeded and mulched.
1786677391 2006-09-21 Union Drilling has finished drilling and is starting to move off site.
1827656906 2010-08-03 Annual inspection of this solution mining well found no violations at this time.