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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-003-22512 | | Well ID: 37-003-22512 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.664681, -79.7141 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 17: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | License Status: | + | | License Status: |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: |
|- | |- | ||
| Permit Date: | | Permit Date: | ||
+ | |- | ||
+ | | Well Type: GAS | ||
|- | |- | ||
| Unconventional Well: N | | Unconventional Well: N | ||
|- | |- | ||
| Configuration: Vertical Well | | Configuration: Vertical Well | ||
+ | |- | ||
+ | | Conservation: No | ||
|- | |- | ||
| Latitude: 40.664681 | | Latitude: 40.664681 | ||
Line 49: | Line 53: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
+ | <!--== Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Date | ||
+ | !scope="col" | Event | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Job Start Date | ||
+ | !scope="col" | Job End Date | ||
+ | !scope="col" | True Vertical Depth (ft) | ||
+ | !scope="col" | Total Water Volume (gal) | ||
+ | !scope="col" | Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Trade Name | ||
+ | !scope="col" | Supplier | ||
+ | !scope="col" | Purpose | ||
+ | !scope="col" | Ingredient Name | ||
+ | !scope="col" | CAS Number | ||
+ | !scope="col" | Additive Percentage by Mass | ||
+ | !scope="col" | Job Percentage by Mass | ||
+ | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Stimulation Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Stimulation Date | ||
+ | !scope="col" | Phase Number | ||
+ | !scope="col" | Chemical Agent | ||
+ | !scope="col" | Volume (gal) | ||
+ | !scope="col" | Treating Pressure (psi) | ||
+ | !scope="col" | Breakdown Pressure (psi) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
<!--== Production Data == | <!--== Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 65: | Line 112: | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | Period | !scope="col" | Period | ||
+ | !scope="col" | Operator | ||
!scope="col" | Waste Type | !scope="col" | Waste Type | ||
!scope="col" | Quantity | !scope="col" | Quantity | ||
Line 140: | Line 188: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
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==References== | ==References== | ||
<references/> | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Pennsylvania Wells]] | [[Category:Pennsylvania Wells]] |
Well ID: 37-003-22512 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Allegheny | |
Municipality: Harrison Township | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: | |
License Status: | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.664681 | |
Longitude: -79.7141 |
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2724872 | Primary Facility | 2018-03-15 | Routine/Complete Inspection | No Viols - Permanently Shut Down | Abandoned gas well found during excavation work on construction site. Wellhead is intact and consists of 13" with cement in collar, 6 5/8" casing open, but sealed off, 4 1/2" casing on casing clamp, swaged to 2 3/8" tubing, valved, teed with tapped plug and needle valve, side is plugged. Well is situated on open hillside. |
2725058 | Primary Facility | 2018-05-01 | Plugging(Includes Plugged/Mined Through) | No Viols - Permanently Shut Down | Keystone Wireline logged well, found TD to be 2852', casing to 1688'. Rig TIH with work string, set two bottom hole plugs in open hole to estimated ~1700'. TOOH with work string. |
2725649 | Primary Facility | 2018-05-02 | Plugging(Includes Plugged/Mined Through) | No Viols - Permanently Shut Down | Keystone Wireline unseated packer and pulled all 1024' of the 4 1/2" casing. TIH with wireline, tagged TOC plug at 1630'. Pulled on 6 5/8" casing, but got no stretch. Ran CBL and found several deep and shallow tight spots. Rigging up to run and set CIBP in bottom of 6 5/8" casing. Will perf casing before cementing to surface. |
2726127 | Primary Facility | 2018-05-03 | Plugging(Includes Plugged/Mined Through) | No Viols - Permanently Shut Down | Keystone set CIBP in 6 5/8" casing and perforated late yesterday. The remaining cement plug to surface was pumped today. Well took cement, requiring an extra 10 sacks cement to maintain cement at surface. |
For data sources see[4]