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__NOEDITSECTION__ | __NOEDITSECTION__ | ||
+ | [[Category:Wells]] |
Well ID: 37-063-25783 | Loading map...
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Operator Name: EXCO RESOURCES PA LLC | |
First Permit Date: 1980-10-10 | |
Last Permit Date: 1980-10-10 | |
Spud Date: 1980-12-09 | |
Unconventional: No | |
Horizontal: No | |
Violations: None | |
Latitude: 40.684601 | |
Longitude: -79.074751 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2013-0 | 1876.0 | 303.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-0 | 2510.0 | 366.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-0 | 3063.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-0 | 3426.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2009-0 | 3641.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2008-0 | 3350.78 | 366.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2007-0 | 3257.0 | 304.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2006-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2006-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2005-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-0 | PRODUCED FLUID | 80.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PARW00001645 | DANCO INDUSTRIES TRMT FAC | HARRISVILLE | PA |
2012-0 | PRODUCED FLUID | 80.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY | JOSEPHINE | PA |
2009-0 | BRINE | 520.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | HART RESOURCE TECH PLT | |||
2009-0 | BRINE | 520.0 | Bbl | OTHER | NOT LISTED | |||
2010-0 | PRODUCED FLUID | 160.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PARW00001645 | DANCO INDUSTRIES TRMT FAC | HARRISVILLE | PA |
2010-0 | PRODUCED FLUID | 163.0 | Bbl | INJECTION DISPOSAL WELL | PAS2D032BARM | DANDO #1 DISPOSAL WELL (005-21675) | INDIANA | PA |
2010-0 | PRODUCED FLUID | 10.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY | JOSEPHINE | PA |
2010-0 | PRODUCED FLUID | 30.0 | Bbl | STORAGE PENDING DISPOSAL OR REUSE | STORAGE PENDING DISPOSAL OR REUSE | PA | ||
2011-0 | PRODUCED FLUID | 80.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PARW00001645 | DANCO INDUSTRIES TRMT FAC | HARRISVILLE | PA |
2012-0 | PRODUCED FLUID | 80.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PARW00001645 | DANCO INDUSTRIES TRMT FAC | HARRISVILLE | PA |
2012-0 | PRODUCED FLUID | 80.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY | JOSEPHINE | PA |
2013-0 | PRODUCED FLUID | 45.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1884580 | 2010-05-11 | No Violations Noted | Inspection conducted with Rick Hoover of DEP, and operator representatives Don Henry, Andy Koval, etc..
Well tag in place. Well equipped for production. Pump jack installed. Access road stable Inspected in response to minor discharge from tank reported to the department by the operator on 5/7/10. Small amount of oil overflowed from the production fluids tank to the ground around the tank and then down-slope approximately 30 feet. Clean up and remediation was immediately initiated by the operator. All contaminated soil was removed and placed in a roll back for disposal at a landfill. All disturbed soil was seeded and mulched. No evidence of any discharge to waters of the commonwealth. Tank appeared sound.
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