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== Well Details == | == Well Details == | ||
{| class="wikitable" width="95%" | {| class="wikitable" width="95%" | ||
− | | Well ID: 125-24035 | + | | Well ID: 42-125-24035 |
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.277777, -80.472333 | width=100% | height=100% }} | | style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.277777, -80.472333 | width=100% | height=100% }} | ||
|- | |- | ||
Line 134: | Line 134: | ||
| Marcellus/Horizontal | | Marcellus/Horizontal | ||
− | All three wells on location 125-24033, 125-24034, & 125-24035 were shut in at the time of investigation/inspection. My purpose for being on location was to gather information from a technical perspective for the department's bureau of investigations. I observed no violations during the course of my investigation, and had the cooperation of everyone on location. | + | All three wells on location 42-125-24033, 42-125-24034, & 42-125-24035 were shut in at the time of investigation/inspection. My purpose for being on location was to gather information from a technical perspective for the department's bureau of investigations. I observed no violations during the course of my investigation, and had the cooperation of everyone on location. |
My remarks on the following page detail my investigation. The following documents that I collected that day are in the possession of the bureau of investigations: Site roster at the time of the fire, tank strap information, and a timeline of events from spud through flowback up to the time of the fire. | My remarks on the following page detail my investigation. The following documents that I collected that day are in the possession of the bureau of investigations: Site roster at the time of the fire, tank strap information, and a timeline of events from spud through flowback up to the time of the fire. | ||
Line 146: | Line 146: | ||
| Marcellus/Horizontal | | Marcellus/Horizontal | ||
− | All three wells on location 125-24033, 125-24034, & 125-24035 were shut in at the time of investigation/inspection. My purpose for being on location was to gather information from a technical perspective for the department's bureau of investigations. I observed no violations during the course of my investigation, and had the cooperation of everyone on location. | + | All three wells on location 42-125-24033, 42-125-24034, & 42-125-24035 were shut in at the time of investigation/inspection. My purpose for being on location was to gather information from a technical perspective for the department's bureau of investigations. I observed no violations during the course of my investigation, and had the cooperation of everyone on location. |
My remarks on the following page detail my investigation. The following documents that I collected that day are in the possession of the bureau of investigations: Site roster at the time of the fire, tank strap information, and a timeline of events from spud through flowback up to the time of the fire | My remarks on the following page detail my investigation. The following documents that I collected that day are in the possession of the bureau of investigations: Site roster at the time of the fire, tank strap information, and a timeline of events from spud through flowback up to the time of the fire | ||
Well ID: 42-125-24035 | Loading map...
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County: Washington | |
Municipality: Independence Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Farm/Lease Name: JOSEPH POWERS 5H | |
First Permit Date: 2010-03-29 | |
Last Permit Date: 2010-03-29 | |
Spud Date: 2010-04-05 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 2 | |
Latitude: 40.277777 | |
Longitude: -80.472333 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1879914 | 2010-04-02 | No Violations Noted | Well spud, site and location good, closed loop system to be used | |
1894203 | 2010-06-23 | No Violations Noted | ||
1915527 | 2010-09-15 | No Violations Noted | Nomak 241 - TD @ 6314, building curve, site and location good, closed loop | |
1933385 | 2010-09-29 | No Violations Noted | ||
1939919 | 2010-09-23 | No Violations Noted | ||
1947845 | 2010-12-01 | Viol(s) Noted & Immediately Corrected | 604166 | |
1947845 | 2010-12-01 | Viol(s) Noted & Immediately Corrected | 604166 | |
1947845 | 2010-12-01 | Viol(s) Noted & Immediately Corrected | 604167 | |
1947845 | 2010-12-01 | Viol(s) Noted & Immediately Corrected | 604167 | |
1952716 | 2011-02-24 | No Violations Noted | ||
1952722 | 2011-02-25 | No Violations Noted | ||
1957130 | 2011-02-23 | No Violations Noted | 19:08 hrs ¿ received call from Jim Russell on site Operations Manager for Chesapeake that fire was in progress in the frac tank area and three workers were injured.
19:10 hrs ¿ received 2nd call from Mike Arch Oil and Gas Inspector supervisor of fire on a Chesapeake Well site. 19:55 hrs ¿ Oil and Gas Inspector Don Rugh arrived at entrance to well site. Access road is approximately ¾ mile long. Multiple fire companies were at site, perimeter control was in place and emergency equipment was being controlled from this point. At this time I started calls to Mike Arch with updates every 15 minutes |
|
1957878 | 2011-02-25 | No Violations Noted | Marcellus/Horizontal
All three wells on location 42-125-24033, 42-125-24034, & 42-125-24035 were shut in at the time of investigation/inspection. My purpose for being on location was to gather information from a technical perspective for the department's bureau of investigations. I observed no violations during the course of my investigation, and had the cooperation of everyone on location. My remarks on the following page detail my investigation. The following documents that I collected that day are in the possession of the bureau of investigations: Site roster at the time of the fire, tank strap information, and a timeline of events from spud through flowback up to the time of the fire.
|
|
1957881 | 2011-02-25 | No Violations Noted | Marcellus/Horizontal
All three wells on location 42-125-24033, 42-125-24034, & 42-125-24035 were shut in at the time of investigation/inspection. My purpose for being on location was to gather information from a technical perspective for the department's bureau of investigations. I observed no violations during the course of my investigation, and had the cooperation of everyone on location. My remarks on the following page detail my investigation. The following documents that I collected that day are in the possession of the bureau of investigations: Site roster at the time of the fire, tank strap information, and a timeline of events from spud through flowback up to the time of the fire |
|
2096914 | 2012-08-31 | No Violations Noted |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-3 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2011-1 | FRACING FLUID WASTE | 110.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR DRILLING OR PLUGGING | PA | ||
2011-2 | FRACING FLUID WASTE | 330.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE OF BRINE TO FRAC A WELL | |||
2012-1 | PRODUCED FLUID | 129.67 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |