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34-031-24246

Well Details

Well ID: 34-031-24246
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Country: United States
State: Ohio
County: Coshocton
Municipality: Tiverton Township
Operator Name: CHEVRON APPALACHIA LLC
Well Pad ID:
Farm/Lease Name: HAINES
License Status: Final Restoration
License Date: 2003-08-14
Spud Date: 1981-04-22
Spud Drilling Contractor:
Final Drill Date: 1981-04-21
Well Total Depth: 3530.00 ft
Configuration: Vertical
Latitude: 40.420000
Longitude: -82.090000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-12-31 1177 ENERGY DISTRIBUTORS INC GeoDate 12/31/80
Oil and Gas 1980-12-31 Issued Date 12/31/80 Expired Date Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1981-04-21
Reached Total Depth 1981-04-21
Original Spud 1981-04-22
CO 1992-06-16 3071 KINGSTON OIL CORP GeoDate 12/31/80
Change of Owner 2001-01-12 Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC
APP 2003-08-14 Proposed Formations:CLINTON, Issued Date:8/14/2003, Expired Date:8/13/2004 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2003-08-29
Construction Permit Expires 2004-08-13
Record Last Modified 2013-03-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3404 3450 18
3404 3450 18
3404 3450 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RPJ FUND MANAGEMENT INC 980.00 337.00 0
1987 ENERGY DISTRIBUTORS INC 246.00 0.00 0
1988 KINGSTON OIL CORP 746.00 157.00 0
1989 KINGSTON OIL CORP 326.00 0.00 365
1990 KINGSTON OIL CORP 0.00 78.00 365
1991 KINGSTON OIL CORP 0.00 77.00 365
1992 KINGSTON OIL CORP 0.00 72.00 350
1993 KINGSTON OIL CORP 0.00 74.00 350
1999 KINGSTON OIL CORP 0.00 0.00 0
2000 KINGSTON OIL CORP 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RPJ FUND MANAGEMENT INC Brine 0 0
1987 ENERGY DISTRIBUTORS INC Brine 0 0
1988 KINGSTON OIL CORP Brine 0 0
1989 KINGSTON OIL CORP Brine 0 365
1990 KINGSTON OIL CORP Brine 0 365
1991 KINGSTON OIL CORP Brine 0 365
1992 KINGSTON OIL CORP Brine 0 350
1993 KINGSTON OIL CORP Brine 0 350
1999 KINGSTON OIL CORP Brine 0
2000 KINGSTON OIL CORP Brine 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1543965586 2003-8-27 0:00: PB No Violations
-154396558693303 2003-7-16 0:00: PW No Violations
-154396558695194 2003-8-27 0:00: PB No Violations
-273964031 2003-7-16 0:00: PW No Violations
0034666869 2003-09-02 Production Wells No Violations well plugged , compliance for idle well .
0273964031 2003-07-16 Production Wells No Violations FOLLOW UP TO NOV # -154396558693303 Complaint of idle well . Well has pumping unit ( no motor on unit ) . Storage tanks have wrong identification .
1061999417 2003-08-27 Plug / Plug Back No Violations Bullheaded bottom plug thru 4.5 casing , went in to tag plug tools stopped at 1445 . Hole in casing @ 1445 . Went in hole with tubing to drill out cement and run tubing to bottom to set bottom plug .
1062087786 2003-08-28 Plug / Plug Back No Violations drilling cement out of 4.5 casing .
1216223206 2003-08-25 Production Wells No Violations Rig moving in 8/26/03 . Phone call from plugging co.
1302839971 2003-08-11 Production Wells No Violations Identification posted , Well still idle . Nov due 8/20/03
1543965586 2003-08-27 Plug / Plug Back Violations Noted Complaint of idle well . Well has pumping unit ( no motor on unit ) . Storage tanks have wrong identification . FOLLOW UP 8/27/03 rig on site , plugging started 8/25/03. Well plugged compliance 09/02/2003
1864397576 2003-11-03 Final Restoration No Violations Passed
34666869 2003-9-2 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1543965586 US-OH-114964 2003-07-16 Well shall be plugged

For data sources see[9]

References