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34-067-21089

Well Details

Well ID: 34-067-21089
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County: Harrison
Municipality:
Operator Name: CHEVRON APPALACHIA LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2012-09-02
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.28854236
Longitude: -81.28032043

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-12 24569.0 4623.0
2013-6 35771.0 11864.0
2013-9 64470.0 14484.0
2014-2 48964.0 91.0 7333.0 91.0
2014-1 64422.0 90.0 11130.0 90.0
2014-4 32471.0 92.0 4201.0 92.0
2015-1 27569.0 90.0 4014.0 90.0
2014-3 40556.0 92.0 5418.0 92.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1347548177 2012-09-11 I arrived on location and found crew getting ready to dig location up to start to repair well location.
1348658251 2012-09-16 Arrived on location and found that while conductor hole was being drilled it started to cave-in between the kinsey 1 and the kinsey 2. Company wasn't sure what to do and wanted my recommendation on how to proceed. Going to plug both holes and remove caved-in area and replace with stone.
-1610940420 2012-09-10 Arrived on location by request of operator because the conductor hole collapsed while drilling. Hole is 36 in diameter and was 47' deep. Well caved in at 37' and crew cannot keep it open . Company wants to plug it back to surface with a ready mix truck.
-195961373 2012-08-14 I am on site today to review pad construction.. Silt fence and erosion controls are being used.
2005291591 2013-09-25 On the day of my inspection the site passed preliminary restoration according to 1509.072A.
480427469 2013-09-25 On the day of my inspection the site passed preliminary restoration according to 1509.072A.
56984811 2012-09-10 I am on site today to plug back another well on this pad. While I was waiting on cement trucks the Rat Hole Drilling crew began drilling this well. I feel this well will collapse and should not be drilled with an Auger type rig. Later I received a call from Inspector Grimm who is covering the plug back and he advised that this well had collapsed and will need to be plugged back. This well did collapse to the point that there was no hole to plug back. Inspector Grimm advised them to bring in a deep reaching Backhoe and dig down and then back fill with rock and stone.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.