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34-099-23157

Well Details

Well ID: 34-099-23157
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: R E DISPOSAL LLC
Well Pad ID:
Farm/Lease Name: NORTHSTAR KHALIL (SWIW #11)
License Status: Final Restoration
License Date: 2011-06-28
Spud Date: 2011-08-18
Spud Drilling Contractor: UNION DRLG
Final Drill Date: 2011-10-05
Well Total Depth: 9580.00 ft
Configuration: Vertical
Latitude: 41.080000
Longitude: -80.610000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-06-28 Proposed Formations:KNOX-PRECAMBRIAN, Issued Date:6/28/2011, Expired Date:6/27/2013 12:00:00 PM, Drilling unit acres:6.7, Proposed Well Type:SWD, Proposed Well Class:SWIW
Reached Total Depth 2011-10-05 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Annulus Pressure Monitoring Approved 2011-10-19 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Change of Owner 2011-11-30 Operator changed from 2651, D & L ENERGY INC to 8893, NORTHSTAR #3 LLC
Last Compliance Report 2011-12-28 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Completion Report Received 2012-02-16 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Construction Permit Expires 2012-06-27 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Plugged Back 2013-06-03 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Plugged/Abandoned 2017-10-18 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.
Record Last Modified 2018-08-02 WELL PLUGGED BACK FROM PRECAMBRIAN BASEMENT TO A DEPTH OF 8774 FEET - TET. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2011-10-25 8098 9581 0
8098 9581 0
8098 9581 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1014886680 2011-11-4 0:00: UD No Violations
-1043225526 2011-9-6 0:00:0 DD No Violations
-1056161397 2014-2-4 0:00:0 SW No Violations
-1229627014 2011-10-6 0:00: SW No Violations
-1459055129 2011-12-30 0:00 SW No Violations
-1504231220 2011-12-8 0:00: SW No Violations
-1542236337 2013-7-10 0:00: SW No Violations 1.00
-1636762765 2017-9-26 0:00: SW No Violations 1.00
-1708524894 2013-6-3 0:00:0 PB No Violations
-1720976750 2011-12-15 0:00 SW No Violations
-1879720333 2011-10-10 0:00 SW No Violations
-1945587175 2017-10-7 0:00: PB No Violations 1.00
-1945745803 2012-12-18 0:00 SW No Violations 1.00
-1958412875 2017-10-15 0:00 PB No Violations 5.00
-2090128913 2017-10-17 0:00 PB No Violations 3.50
-223580904 2013-10-31 0:00 SC No Violations
-271809129 2016-3-29 0:00: SW No Violations
-28887163 2011-8-19 0:00: DD No Violations
-316512043 2017-10-3 0:00: PB No Violations 9.00
-359829285 2011-10-24 0:00 UD No Violations
-553169173 2017-10-13 0:00 PB No Violations 5.50
-583523902 2011-9-22 0:00: DD No Violations
-616346790 2011-8-31 0:00: DD No Violations
-629635051 2017-9-28 0:00: PB No Violations 3.50
-666356136 2014-12-30 0:00 SW No Violations
-950722184 2017-10-10 0:00 PB No Violations 1.00
-976980655 2013-5-8 0:00:0 SW No Violations 1.00
0028887163 2011-08-19 Drill / Deepen / Reopen No Violations Butchs Rat Hole and Anchor, drilled a 51 hole and installed/cemented 50 of new 20 conductor.
0160040668 2015-03-27 Salt Water Injection Well No Violations No recent active. Wellhead remains shut-in. No equipment on location. Gate locked at the entrance.
0223580904 2013-10-31 Surface Facility Construction No Violations My inspection was accompanied by Andrew Adgate. There were no changes at the well site.
0271809129 2016-03-29 Salt Water Injection Well No Violations The inspection was a follow-up on Chiefs Order No. 2014-421.

The well was shut-in. There was nothing else onsite. There was no indication of recent activity.

0288192798 2012-06-25 Surface Facility Construction No Violations My inspection found the well idle and no further progress on the facility construction.
0316512043 2017-10-03 Plug / Plug Back No Violations Team Energy ran 280 joints of 2-3/8 tubing and tagged bottom at 8791 set tubing at 8780. C&J Energy Services was the cementers on location to spot the 200 plug they pumped 100 sacks of class H cement 16.4 lb/gal 1.06 yield. Displaced with 31 barrels of fresh water. Pulled 10 joints of tubing and reversed circulated 68 barrels to clear tubing. 1 barrel of cement to surface. Left location shut down for 8 hr. for cement strength before tagging the plug. Estimated top of cement is 8580
0359829285 2011-10-24 Urban Drill / Deepen / Reopen No Violations U.D.I. #52 is rigging down and moving off location. The well head is shut in and fenced with orange temporary fencing. No leaks or spills. No violations noted.
0458307282 2017-10-14 Plug / Plug Back No Violations Team Energy drilled to a depth of 5070. Renegade Wireline ran a CBL log inside the 7-5/8 casing from 4500 to 5070. There was no cement bond. I contacted Deputy Chief Bob Worstall and Deputy Chief Dave Claus to discuss the gone forward operation. They requested that Rex Energy run a free point test to find free pipe. KLX arrived on location at 4:15 pm to run free point. Baker Hughes was on location to set the 7-5/8 casing spear. KLX ran to a depth of 3815. Team Energy pulled 196000 pounds of pull but could not unset from the casing seat. After discuss with Deputy Chief Bob Worstall they would install a CIBP plug at 3800 cut 7-5/8 casing at 3700. Remove 7-5/8 casing and process with the plugging plan.
0553169173 2017-10-13 Plug / Plug Back No Violations Team Energy at this time is running the 6.5 convex end mill and will resume the drilling. They tagged the plug at 4903 and will drill to 5089. Waiting on power tong to be repaired.
0583523902 2011-09-22 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling 9-7/8 hole on fluid, at depth of 8138. Changed from polycrystalline-diamond compact (PDC) bit to button bit. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. Running RAM style BOP. Permit displayed at lease road entrance and in office. No violations at this time.
0616346790 2011-08-31 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling surface hole on fluid, at depth of 721. Reported problems down hole with buried trash and debris. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. No violations at this time.
0618551485 2011-09-13 Urban Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling 9-7/8 hole on fluid, at depth of 4824. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. Running RAM style BOP. Permit displayed at lease road entrance and in office. No violations at this time.
0629635051 2017-09-28 Plug / Plug Back No Violations I performed an inspection of the location. They are moving equipment and office trailers on location to prepare for the plugging of this well. Wicklow Logistics had two water trucks hauling fresh water into the 500 barrel frack tank to be used for the plugging. I looked up there UIC number 25-639 and discovered that they were on hold for not reporting there 2016 reports. I contacted Derk Smith from Rex Energy and informed him that could not haul salt brine in Ohio until they resolve this issue.
0666356136 2014-12-30 Salt Water Injection Well No Violations The well remains shut-in. There was no indication of recent activity.
0686502932 2013-10-15 Salt Water Injection Well No Violations There were no changes at the well site and no sign of activity.
0686817616 2017-10-12 Plug / Plug Back No Violations At present Rex Energy and Team Energy are in the process drilling out the cement retainer and 4860 to 5020. The were using a 6.5 tri-cone bit could not cut the (CIBP) Cast Iron Bridge Plug. At present they are tripping out of the well and will be installing a 6.5 convex end mill and resume the drill out.
0838112005 2013-10-29 Salt Water Injection Well No Violations I performed a status check on the above location. Gates are locked. At present there is no active at this location.
0839593739 2017-10-05 Plug / Plug Back No Violations Team Energy pulled the tubing out of the well to confirm the pipe depth at 8073 and ran back in the well to a total depth 8670. Before setting down on the cement plug (121plug).The tubing was setting down on the two packers when checking for the cement top.
0919192678 2017-10-12 Plug / Plug Back No Violations At present Rex Energy and Team Energy are in the process drilling out the cement retainer and 4860 to 5020. The were using a 6.5 tri-cone bit could not cut the (CIBP) Cast Iron Bridge Plug. At present they are tripping out of the well and will be installing a 6.5 convex end mill and resume the drill out.
0950722184 2017-10-10 Plug / Plug Back No Violations Larry Boone notified me at 1:30 am of the cement top at 6917 (578 plug). I gave them the permission to proceed with the plugging plan that was discussed. I was on location at 8:16 am. They were tripping out of the well with the tubing. Renegade Wireline Service will be on location to set Cast Iron Bridge Plug (CIBP) at 5495. They perforated at 5481-5485 and 5382-5385 and set a cement retainer at 4900.
0976980655 2013-05-08 Salt Water Injection Well No Violations My inspection found no activity on site. No additional work has been done on the facility.
1014517282 2017-03-30 Salt Water Injection Well No Violations No attempt has been made to construct the surface facility. There were no noticeable changes on location, since the last inspection. There was no indication of recent activity.
1014886680 2011-11-04 Urban Drill / Deepen / Reopen No Violations All drilling equipment has been removed from location. The well head is shut in and fenced. There are no open pits. I took GPS readings on the well head. No leaks or spills. Security guard on duty. No violations at this time.
1043225526 2011-09-06 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling on fluid, at depth of 3851. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. No violations at this time.
1056161397 2014-02-04 Salt Water Injection Well No Violations There were no changes found on site.
1080997959 2013-05-31 Salt Water Injection Well No Violations Rex Energy is in the process of filling six 500 barrel frac tanks to be used in there injection test on the above location. As I was on location there was a truck hauling brine came on location ( Wes Baker Trucking #903 ) this truck was not registered with the UIC Division of ODNR. I instructed him that he could not haul brine in Ohio with out been regisitered with the UIC Division. I called Deputy Chief Robert Worstall about this. He called Sean Wessert from Rex Energy and also informed him. The tanks were filled by a registered hauler.
1085187645 2017-06-05 Salt Water Injection Well No Violations The injection well and wellsite were inspected. No change since last inspection and no sign of recent activity. The facility remains incomplete and the well was never hooked-up.
1098991380 2016-09-07 Salt Water Injection Well No Violations The inspection was a follow-up on Chiefs Order No. 2014-421.

The well was shut-in. There was no indication of recent activity.

1117361101 2013-06-10 Salt Water Injection Well No Violations I was on location with UIC Inspector Steve Ochs during the injection test. See Steves report.
1139503527 2012-08-23 Salt Water Injection Well No Violations My inspection of the well site and injection facility was accompanied by another inspector, John Fleming.

The well was not in operation. The facility construction remains incomplete. The preliminary restoration needs finished.

John Fleming notifie

1229627014 2011-10-06 Salt Water Injection Well No Violations On site with inspector Carl Roberts to witness the running and testing of the 5 injection string and packer. Union Drilling Rig #52 having problems running packer. Have to order a different packer. No leaks or spills. No violations at this time.
1232297637 2014-09-15 Salt Water Injection Well No Violations There was no sign of recent activity. No apparent changes on location.
1288079659 2013-01-14 Salt Water Injection Well No Violations My inspection found no activity on site. No additional work has been done on the facility.
1299988032 2014-06-30 Salt Water Injection Well No Violations An inspection of the well site found no recent sign of activity. The well remains shut-in and disconnected. The surface facility construction has not started.
1315493379 2011-09-02 Drill / Deepen / Reopen No Violations I was on site for the cementing of the surface casing on Union Rig #52. Universal Well Service on site to cement. Union drilled a 13.5 hole to a total depth of 1025. The surface pipe is new 10.5 J55, R-3 40.5 pounds/foot pipe. Union set surface pipe at 1019 KB (1003 in the ground). They ran a guide shoe, float collar and 15 centralizers on the casing. The centralizers were set on every other joint. Universal ran 150 pounds of Sweep in 1000 gallons of fresh water, 1000 pounds of gel and two sacks of unicele ahead of the cement. They then ran 449 sacks of Class A cement with 3% CaCl, 2% foam reducer and 1/4 sack of unicele. They displaced the cement to 940. Displacement volume was 92.2 barrels. There was 30 barrels of good cement returned to surface. Sweep is sodium acid pyrophosphate and is listed as non-hazardous on the MSDS. Cement water pH was 8.
1318423916 2011-10-05 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 reached total depth of 9581 with 9-7/8 hole. Set 8098 of 7-5/8 casing. Met with Aaron Wilhite to discuss details of running 5 injection string, setting and testing packer. No leaks or spills. No violations at this time.
1319037130 2011-10-19 Salt Water Injection Well No Violations On site to witness packer being run into hole. Inspected packer before it went into hole. Packer is a new Baker Lockset T-440 ID 5 inch OD 6.75 inch. Team Oil Tools on location to supervise running of the packer. Packer will be set at 7990. Operator to shoot off Weatherford permanent packer at 7993. The Baker packer will be set three feet above the Weatherford packer. Pipe is new 4.5 Grade P-110 API, R-3, 13.5 pound pipe. Express on site to torque pipe. Carl Roberts on site for relief.
1319209919 2011-10-10 Salt Water Injection Well No Violations I was on site for the packer pressure test. The operator dropped the ball too expand the packer. Total depth of this well was 9581, with 7.625 casing set at 8098. The packer was set at 8013 and the 5 casing was set at 7971. The 1st test was conducted using the ODNR gauge: Operator pressured up to 2000 PSI. A valve was leaking and the annulus lost 100 PSI in 4min 34 seconds - test failed. 2nd test: Annulus charged to 2000 PSI and the annulus lost 200 PSI in 4 minutes 52 seconds - test failed. The ODNR gauge was leaking at the fitting because it has 3/8 threads and was threaded onto a 1/2 nipple provided by the rig. The 3rd test performed using the service company gauge: Annulus charged to 2050 PSI and lost 300 PSI in 15 minutes - test failed. The operator dropped 2nd ball to confirm that the packer had been expanded. The ball pressured to 1720 PSI and there was 50 PSI on the annulus. 4th test: Annulus charged to 2700 PSI. After 5 minutes the annulus pressure was 2550 PSI and after 14 minutes the annulus pressure was 2250 PSI - test failed. 5th test: Annulus charged to 2000 PSI. After 13 minutes the annulus pressure was 1725 PSI - test failed. There was a flow of fluid coming out of the 5 casing. When the annulus was pressurized the flow increased and when the pressure was released the flow decreased. The operator was informed to contact me when corrections have been made to the packer and they were ready to re-start the test.
1323714411 2011-12-06 Salt Water Injection Well No Violations Appalachian Well Survey was on site to run the gamma ray-collar locator correlation log. This is being done prior to completing the RAT and the step test on 12/8. No violations at this time.
1324384483 2011-12-17 Salt Water Injection Well No Violations I witnessed the UIC test again with Rex Resources. Superior preformed the UIC test. A permanent 7.625 packer had been set at 8045 with one joint of tail pipe below. On 10/17/11 the top of the packer was shot off leaving the packer and tail pipe in the hole. On 10/19/11 a Lok-Set packer and 4.5 casing was run into the hole and set in 30,000 PSI compression. This packer had failed during a pump rate test around 12/7/11 due to the rubbers relaxing causing the failure. On 12/17/11 the UIC was tried again with Superior pressuring up the annulus to 2000 PSI. Pressure loss was 13 PSI in 15 minutes. The UIC test passed.
1325859959 2012-01-03 Salt Water Injection Well No Violations I was on location to follow up on the annular pressure blow down completed on 12/30/2011. The annular pressure is holding at 500 PSI. The injection casing pressure is at 0 PSI. No leaks or spills were noted.
1333741633 2012-03-14 Salt Water Injection Well No Violations There were no violations at the time of inspection. Forms were installed for the concrete pad. There were no signs of recent work.
1346949207 2012-08-23 Salt Water Injection Well Violations Noted On 8/23/2012, DNR Inspector Steve Ochs and myself did an inspection on the above location. This site has not been reclaimed. This is an Urban Location Per HB 165. The reclamation need to be completed within 30 days of 9/6/2012.
1348240076 2012-09-18 UrbanPreliminary Restoration No Violations On 9/18/2012, North Region Manager Tom Hill and myself met with Rex Energies Personal at the above location to discuss the restoration of the location. They are in the legal phase of getting total control of this location. We agreed to let them put a gate with a lock and identification sign at the entrance of the location, check all silt fence around location repair if needed and also install a fence around a large hole 10 wide x 10 long 5 deep.
1350328540 2012-10-11 UrbanPreliminary Restoration No Violations My inspection of the above location found: They have installed an entrance gate. Repaired the silt fence. Installed and replace sections of the security fence. They fenced in a large 10 by 10 by 4 deep hole. The compliance Notice is passed 10/11/2012
1373472746 2013-06-10 Salt Water Injection Well No Violations An injection test was performed on the well. A total of 649 barrels of brine were pumped in one hour and forty-five minutes.

John Fleming was also onsite. All conditions were acceptable.

1380811969 2013-08-15 Administrative Inspection No Violations I meet with Deputy Chief Bob Worstall at the above location. We performed a status check on this location, at present there is no activity. The location is secured with a locked gate at the entrance of the location. Well head is locked out. No notied violation at this time.
1399487967 2011-09-06 Drill / Deepen / Reopen No Violations Tom Hill, Chris Grimm and myself performed a rig inspection on Union rig #52. The drilling depth was 3581 and drilling on fluid. The zone was Newburg. This inspection satisfies 1501:9-9-03. There were no violations at this time.
1450721801 2015-12-17 Salt Water Injection Well No Violations I performed a status check on the above location. There is no active at this time on this location. Location is secured gates are locked.
1459055129 2011-12-30 Salt Water Injection Well No Violations I was called out to witness annular pressure being blown down. The pressure gauge reading was 2800 PSI on the annulus at the time of my arrival. A Rex Energy representative opened up the annulus and blew down the pressure to 500 PSI. Blow down took approximately 5 minutes after which the well was shut in. Annular pressure holding at 500 PSI, injection string pressure at 0 PSI.
1478865821 2011-09-29 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling 9-7/8 hole on fluid, at depth of 9249. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. Running RAM style BOP. Permit displayed at lease road entrance and in office. No violations at this time.
1504231220 2011-12-08 Salt Water Injection Well No Violations This well was drilled to a total depth (TD) of 9,581 with 7.625 casing set at 8,094 and 10.75 surface casing set at 1,016. The 4.5 casing packer was set at 7,968. The salt water injection zone extends from the bottom of the 7.625 casing to TD and includes the following formations, Knox, Rose Run, Copper Ridge, Conasauga, Rome, Mount Simon, granite wash and Precambrian basement. The purpose of todays actions were to determine where in this sequence the injected brine was going. On site personnel and contractors included Larry Smyers and Dave Jenkins (D&L Energy), Larry Shamblin (Core Laboratories) and Superior Well Service personnel providing a frac van, pump trucks, crane truck and field hands, and Appalachian Well Surveys providing open hole and cased hole logging tools.

Step I - On 12/6 Appalachian ran a gamma ray log to correlate with the open hole nuclear logs completed during the drilling phase. The gamma ray tool was run inside of the 4.5 casing set at 7,968 and into open hole. A new logger TD was established at 9,488 which is 93 shallower than the TD noted on the original drillers TD. This new depth places the bottom of the hole just below the Precambrian basement.

Step II - On 12/8 Core Lab placed radioactive ceramic beads (Scandium 46) in the top of the 4.5 casing and Superior Well Services displaced the beads using 288 barrels of brine at a rate of 3 to 7 barrels per minute (bpm). This volume was calculated as hole/casing capacity plus 10 barrels. The maximum injection pressure was 1700 pounds per square inch (psi) during initial displacement. Instantaneous Shutin Pressure (ISIP) was 1250 psi and after 5 minutes, pressure stayed at 1250 psi.

Step III - After the beads had been displaced and the pressure reduced on the well, Appalachian ran the gamma ray tool with collar locator to the bottom of the hole to quantify the bead distribution through the injection zone. (Refer to the log copies) The results indicated that the beads were di

1509377188 2017-10-02 Plug / Plug Back No Violations Team Energy was on location to perform the plugging operations of this well. I met with Rex Energys Consultants Larry Boone and Arron Wilhite about the plugging of this well. At present they are laying containment for the pipe handler to set on and the service rig and pipe racks. Gas monitoring H2S equipment was installed at the rig by the well head. There was a manifold and flare stack installed also. Tubing will be drifted and strapped. 280 joint of 2-3/8 tubing 8791.
1509453332 2017-10-11 Plug / Plug Back No Violations Renegade Wireline Service ran a CBL log. The log shows no cement bond from 3500 to 4860. Rex Energy proposed a plan to drill cement from 4900 5020. Renegade will run a CBL to check cement bonding if no bonding ODNR will review a plan that Rex Energy propose.
1511190707 2017-10-06 Plug / Plug Back No Violations Team Energy tripped 2-3/8 tubing in the well and tagged cement at 8095. (578 plug). Waiting on C&J Energy Services. They established circulation pumped a 201 plug 20 sks of class H cement and displaced with 40 bbls of fresh water. Will tag cement top in 8 hours.
1532545944 2018-07-25 Final Restoration No Violations I performed a Final Restoration inspection on the above location. No Drilling or Production Equipment is on location well has been plugged 10-17-2017. Final Restoration is passed. No Violations.
1542236337 2013-07-10 Salt Water Injection Well No Violations I performed a status check on the above location. The 500 barrel frac tanks that were on location has been removed. At this time there is know activity on location. Gates are locked.
1581458141 2011-09-27 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling 9-7/8 hole on fluid, at depth of 9033. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. Running RAM style BOP. Permit displayed at lease road entrance and in office. No violations at this time.
160040668 2015-3-27 0:00: SW No Violations 1.00
1605812389 2011-09-20 Drill / Deepen / Reopen No Violations Union Drilling Rig #52 drilling 9-7/8 hole on fluid, at depth of 7801. Drilling in Black River Limestone. Oil/gas show in Utica Shale. Gravel drilling pad enclosed with chain link fencing, security guard on duty, steel pits, closed loop mud system, no leaks or spills. Running RAM style BOP. Permit displayed at lease road entrance and in office. No violations at this time.
1636762765 2017-09-26 Salt Water Injection Well No Violations I performed a status check on the above location. The well is not in operation. At this time the location is being prepared to plug the well. There is security on location.
1702611826 2017-10-04 Plug / Plug Back No Violations I received a phone call from Larry Boone stating that they tagged the cement top at 8073 500 high. I meet with Deputy Chief Dave Claus and North East Region Manager Steve Ochs and Andrew Adgate to discuss this issues. The were instructed that they would need to drill out the cement and install a new cement plug.
1708524894 2013-06-03 Plug / Plug Back No Violations My inspection of the plug-back operation was accompanied by John Fleming. The well was plugged from 9504 feet to 8773 feet, through coil tubing, using 295 sacks Class-A cement. The well site and cement operation met all requirements.

Later, the plug was tagged at 8773 feet. One foot of the plug was drilled, leaving the new total depth at 8774 feet.

1720976750 2011-12-15 Salt Water Injection Well No Violations I witnessed a partial running into the hole with the 4.5 casing injection string. I also witnessed the UIC test. The hole was already filled with packer fluid, since the packer was left in the hole. Only the on/off tool was replaced. The 7 Baker 600-292 Hornet packer has been set at 7875 (top) and 7882 (bottom). The workover rig had pumped 155 barrels of packer fluid down the annulus and up the tubing. The annulus was then pressured up to 2000 PSI and it held for 15 minutes. The UIC passed. There were no violations at this time.
1879720333 2011-10-10 Salt Water Injection Well No Violations On site with inspector Tom Hill to witness the pressure testing of the packer and 5 casing. Pressure test failed five (5) times. Aaron Wilhite instructed to call when ready to test again. No leaks or spills. No violations at this time.
1916999940 2017-10-16 Plug / Plug Back No Violations Team Energy ran 121 joints of 2-3/8 tubing and tagged the CIBP at 3800. They circulated the well bore with 400 bbls of fresh to balance the well before setting the next plug. C&J Energy services pumped 5 bbls class A cement 15.6 lb/gal 1.18 yld. And displaced with 11 bbls of fresh water. Tagged cement top at 3173
1945587175 2017-10-07 Plug / Plug Back No Violations Larry Boone notified me at 1:30 am of the cement top at 6917 (578 plug). I gave them the permission to proceed with the plugging plan that was discussed. I was on location at 8:16 am. They were tripping out of the well with the tubing. Renegade Wireline Service will be on location to set Cast Iron Bridge Plug (CIBP) at 5495. They perforated at 5481-5485 and 5382-5385 and set a cement retainer at 4900.
1945745803 2012-12-18 Salt Water Injection Well No Violations I performed an inspection at the above location. This well is not in operation at this time.
1958412875 2017-10-15 Plug / Plug Back No Violations Renegade Wireline set CIBP at 3800. Renegade Wireline cut the 7-5/8 casing at 3700. Team Energy pulled 7-5/8 casing and tally casing.
2090128913 2017-10-17 Plug / Plug Back No Violations I was on location to witness the cement top at the surface plug. There was a 10-3/4 CIBP set at 700 and a 700 cement plug the plug was there. They cut the well head off 6 below grade and welded a cap with ID number. Tin horn was removed cellar was filled with lime stone. Equipment is in the process of being removed. Will meet with a representative from Rex Energy to walk and clear location.
2116745477 2015-07-24 Salt Water Injection Well No Violations The inspection was a follow-up on Chiefs Order No. 2014-421.

There were no changes onsite, since the last inspection.

288192798 2012-6-25 0:00: SC No Violations
458307282 2017-10-14 0:00 PB No Violations 6.50
618551485 2011-9-13 0:00: UD No Violations
686502932 2013-10-15 0:00 SW No Violations
686817616 2017-10-12 0:00 PB No Violations 5.50
838112005 2013-10-29 0:00 SW No Violations 1.00
839593739 2017-10-5 0:00: PB No Violations 8.00
919192678 2017-10-12 0:00 PB No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1346949207 US-OH-110052 2012-09-06 FENCING (a-d)
1346949207 US-OH-110053 2012-09-06 Failure to restore land surface within 9 mos.

For data sources see[4]

References