X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-153-20738

Well Details

Well ID: 34-153-20738
Loading map...
Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: GOODYEAR TIRE & RUBBER
Well Pad ID:
Farm/Lease Name: COOK R F
License Status: Final Restoration
License Date: 2014-06-26
Spud Date: 1980-01-03
Spud Drilling Contractor:
Final Drill Date: 1980-01-07
Well Total Depth: 3967.00 ft
Configuration: Vertical
Latitude: 41.190000
Longitude: -81.470000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-10-09 518 GOODYEAR TIRE & RUBBER GeoDate 10/9/79
Original Spud 1980-01-03 ACRES 25.6381
Completed 1980-01-07 ACRES 25.6381
Reached Total Depth 1980-01-07 ACRES 25.6381
APP 2005-01-05 Proposed Formations:CLINTON, Issued Date:1/5/2005, Expired Date:1/5/2006 6:00:00 AM, Drilling unit acres:25.6, Proposed Well Type:OG, Proposed Well Class:
APP 2014-06-26 Proposed Formations:CLINTON, Issued Date:6/26/2014, Expired Date:6/25/2016 12:00:00 PM, Drilling unit acres:25.6381, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-08-06 ACRES 25.6381
Record Last Modified 2014-12-23 ACRES 25.6381
Construction Permit Expires 2015-06-26 ACRES 25.6381

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3764 3806 19
3764 3806 19
3764 3806 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 115000 Gal 40000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 GOODYEAR TIRE & RUBBER 8931.00 0.00 365
1985 GOODYEAR TIRE & RUBBER 8767.00 157.00 0
1986 GOODYEAR TIRE & RUBBER 6165.00 0.00 365
1987 GOODYEAR TIRE & RUBBER 2667.00 75.00 365
1988 GOODYEAR TIRE & RUBBER 2307.00 102.00 365
1989 GOODYEAR TIRE & RUBBER 1858.00 65.00 365
1991 GOODYEAR TIRE & RUBBER 1859.00 0.00 365
1992 GOODYEAR TIRE & RUBBER 2164.00 71.00 365
1993 GOODYEAR TIRE & RUBBER 1139.00 0.00 365
1994 GOODYEAR TIRE & RUBBER 1611.00 0.00 365
1995 GOODYEAR TIRE & RUBBER 1324.00 61.00 365
1996 GOODYEAR TIRE & RUBBER 1477.00 0.00 365
1997 GOODYEAR TIRE & RUBBER 1773.00 60.00 0
1998 GOODYEAR TIRE & RUBBER 1067.00 38.00 365
1999 GOODYEAR TIRE & RUBBER 1717.00 0.00 365
2000 GOODYEAR TIRE & RUBBER 1476.00 0.00 365
2001 GOODYEAR TIRE & RUBBER 1564.00 58.00 365
2002 GOODYEAR TIRE & RUBBER 1729.00 58.00 365
2003 GOODYEAR TIRE & RUBBER 498.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 GOODYEAR TIRE & RUBBER Brine 100 365
1985 GOODYEAR TIRE & RUBBER Brine 0 0
1986 GOODYEAR TIRE & RUBBER Brine 0 365
1987 GOODYEAR TIRE & RUBBER Brine 0 365
1988 GOODYEAR TIRE & RUBBER Brine 0 365
1989 GOODYEAR TIRE & RUBBER Brine 0 365
1991 GOODYEAR TIRE & RUBBER Brine 0 365
1992 GOODYEAR TIRE & RUBBER Brine 0 365
1993 GOODYEAR TIRE & RUBBER Brine 0 365
1994 GOODYEAR TIRE & RUBBER Brine 0 365
1995 GOODYEAR TIRE & RUBBER Brine 129 365
1996 GOODYEAR TIRE & RUBBER Brine 135 365
1997 GOODYEAR TIRE & RUBBER Brine 0
1998 GOODYEAR TIRE & RUBBER Brine 0 365
1999 GOODYEAR TIRE & RUBBER Brine 0 365
2000 GOODYEAR TIRE & RUBBER Brine 0 365
2001 GOODYEAR TIRE & RUBBER Brine 0 365
2002 GOODYEAR TIRE & RUBBER Brine 0 365
2003 GOODYEAR TIRE & RUBBER Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1616848123 2005-3-1 0:00:0 PB No Violations
-1768895449 2014-7-9 0:00:0 PB No Violations 2.50
-454360420 2014-6-25 0:00: PB No Violations 4.00
-510528013 2005-6-21 0:00: PB No Violations
0188619694 2005-11-14 Plug / Plug Back No Violations Arvilla was on site drilling out the cement plugs through the top of the Big Lime in order to re-plug the well. The well leaked after it was plugged a year ago. Drilling will be completed today and plugging is scheduled for tomorrow morning.
0454360420 2014-06-25 Plug / Plug Back No Violations I met with Inspector Bob Roush and Keith and Jeff Moore at Moores offices in Stow to discuss the drill-out and re-plugging of this leaking well. Operations should commence on 7/7/14. Inspector Roush and I also inspected the location to locate the well. No violations.
0510528013 2005-06-21 Plug / Plug Back No Violations There has been no change since the last inspection. The well is still leaking and will need to be drilled out and replugged. Waiting on a service rig.
0962338309 2005-05-09 Plug / Plug Back No Violations The well was plugged on 2/16/2005. During a status check inspection before granting final restoration, the well was found to be leaking gas. I contacted Karen Burlingame with Goodyear and told her that they needed to expose the wellhead to determine the location of the leak. She then contacted Randy Ile with Arvilla who will arrange for a backhoe to expose the well.
1107889456 2005-02-07 Production Wells No Violations Status check inspection prior to plugging the well. No violations at this time.
1116893497 2005-05-16 Plug / Plug Back No Violations Arvilla personel uncovered the wellhead. It appears that the gas is leaking up through the casing. Arvilla is working on a proposal to Goodyear to drill out and replug the well.
1414761580 2014-10-23 Final Restoration No Violations This well was recently replugged after found to be leaking. Upon my inspection I found the no expression of the previous well. The site has been seeded and is growing. All equipment has been removed. The location is stable and absent of any erosional features. The R F Cook # 1 meets all requirements for final restoration.
1616848123 2005-03-01 Plug / Plug Back No Violations The well was recently plugged. The tank battery has been dismantled and moved off site. Still waiting on either the landowner waiver or the removal of the flowline, salesline, and lease road.
1768895449 2014-07-09 Plug / Plug Back No Violations I was on location to check the drill-out status of this plugged and abandoned well. Inspector Norburt Lowder was on location overseeing operations. Moore Resources was currently drilling out the surface plug inside the 8.625 casing. Returns to the circulating tank began showing shards of metal and it was decided to pull out of the hole and inspect the bit. One of the tooth cones on the Rasta bit had unthreaded off of the bit head and would need to be fished. Operations shut down and Moores went to get some heavy rope and a magnet to retrieve the lost cone. No violations.
188619694 2005-11-14 0:00 PB No Violations
2006983965 2003-02-19 Production Wells No Violations Status check inspection. No violations at this time.
962338309 2005-5-9 0:00:0 PB No Violations

For data sources see[9]

References