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34-153-22144

Well Details

Well ID: 34-153-22144
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: EVERFLOW EASTERN PARTNERS LP
Well Pad ID:
Farm/Lease Name: BENDER
License Status: Producing
License Date: 1985-09-09
Spud Date: 1985-09-30
Spud Drilling Contractor: RAPID DRILLING
Final Drill Date: 1985-10-06
Well Total Depth: 3458.00 ft
Configuration: Vertical
Latitude: 41.170000
Longitude: -81.570000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1985-09-09 Issued Date 9/9/85 Expired Date 9/9/86 Acres 0020000 Tool Type RTAF Proposed Formation CLTN/GORDON Proposed Depth 03458 Proposed Drill Depth 03458
Original Spud 1985-09-30
Completed 1985-10-06
Reached Total Depth 1985-10-06
Completion Report Received 1985-12-17
Construction Permit Expires 1986-09-09
CO 1986-12-05 1809 SPENCER PETROLEUM CORP GeoDate 9/9/85
Change of Owner 1999-12-28 Operator changed from 1809, SPENCER PETROLEUM CORP to 2455, WHIDBEY RESOURCES INC
Change of Owner 2001-06-28 Operator changed from 2455, WHIDBEY RESOURCES INC to 6791, NORMAN D INVESTMENTS
Change of Owner 2001-06-28 Operator changed from 6791, NORMAN D INVESTMENTS to 84, EVERFLOW EASTERN PTNS L P
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3299 3391 0
3299 3391 0
2006-09-11 3324 3367 24
3324 3367 24
3299 3391 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 8 150 Gal 0 7 1/2%, HOLLOW STEEL CARRIERS, .039" HOLE DIAMETER
GEL 0 70000 Gal 30000 NOT YET--PRELIMINARY

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 SPENCER PETROLEUM CORP 47338.00 3934.00 342
1988 SPENCER PETROLEUM CORP 42766.00 2195.00 365
1989 SPENCER PETROLEUM CORP 33084.00 1604.00 365
1993 SPENCER PETROLEUM CORP 2320.00 861.00 365
1995 SPENCER PETROLEUM CORP 21737.00 617.00 365
1997 SPENCER PETROLEUM CORP 6149.00 284.00 365
1998 SPENCER PETROLEUM CORP 4055.00 180.00 365
1999 SPENCER PETROLEUM CORP 3228.00 105.00 365
2000 SPENCER PETROLEUM CORP 4462.00 360.00 365
2001 EVERFLOW EASTERN PARTNERS LP 4862.00 128.00 365
2002 EVERFLOW EASTERN PARTNERS LP 6726.00 119.00 365
2003 EVERFLOW EASTERN PARTNERS LP 4153.00 0.00 365
2004 EVERFLOW EASTERN PARTNERS LP 3774.00 256.00 365
2005 EVERFLOW EASTERN PARTNERS LP 1881.00 381.00 365
2006 EVERFLOW EASTERN PARTNERS LP 2083.00 184.00 365
2007 EVERFLOW EASTERN PARTNERS LP 2226.00 151.00 365
2008 EVERFLOW EASTERN PARTNERS LP 2505.00 404.00 365
2009 EVERFLOW EASTERN PARTNERS LP 2088.00 208.00 365
2010 EVERFLOW EASTERN PARTNERS LP 1025.00 310.00 365
2011 EVERFLOW EASTERN PARTNERS LP 4455.00 463.00 365
2012 EVERFLOW EASTERN PARTNERS LP 3221.00 364.00 366
2013 EVERFLOW EASTERN PARTNERS LP 2943.00 325.00 365
2014 EVERFLOW EASTERN PARTNERS LP 1883.00 269.00 365
2015 EVERFLOW EASTERN PARTNERS LP 1835.00 257.00 365
2016 EVERFLOW EASTERN PARTNERS LP 3355.00 358.00 365
2017 EVERFLOW EASTERN PARTNERS LP 2273.00 341.00 365
2018 EVERFLOW EASTERN PARTNERS LP 3274.00 409.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 SPENCER PETROLEUM CORP Brine 185 342
1988 SPENCER PETROLEUM CORP Brine 85 365
1989 SPENCER PETROLEUM CORP Brine 0 365
1993 SPENCER PETROLEUM CORP Brine 35 365
1995 SPENCER PETROLEUM CORP Brine 0 365
1997 SPENCER PETROLEUM CORP Brine 63 365
1998 SPENCER PETROLEUM CORP Brine 153 365
1999 SPENCER PETROLEUM CORP Brine 0 365
2000 SPENCER PETROLEUM CORP Brine 77 365
2001 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2002 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2003 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2004 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2005 EVERFLOW EASTERN PARTNERS LP Brine 30 365
2006 EVERFLOW EASTERN PARTNERS LP Brine 2 365
2007 EVERFLOW EASTERN PARTNERS LP Brine 3 365
2008 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2009 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2010 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2011 EVERFLOW EASTERN PARTNERS LP Brine 78 365
2012 EVERFLOW EASTERN PARTNERS LP Brine 27 366
2013 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2014 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2015 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2016 EVERFLOW EASTERN PARTNERS LP Brine 82 365
2017 EVERFLOW EASTERN PARTNERS LP Brine 42 365
2018 EVERFLOW EASTERN PARTNERS LP Brine 48 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1620647821 2002-10-18 0:00 PW No Violations
-1939228024 2004-10-20 0:00 PW No Violations
0036770624 2002-10-18 Production Wells No Violations Status check inspection - the stuffing box is leaking and has been leaking for some period of time. An area 6 x 6 is heavily stained with free oil. Contacted the operator and the pumper and ordered that the leak be corrected and the spill remediated.
1620647821 2002-10-18 Production Wells Violations Noted FOLLOW UP TO NOV # 367: Status check inspection - the stuffing box is leaking and has been leaking for some period of time. An area 6 x 6 is heavily stained with free oil. Contacted the operator and the pumper and ordered that the leak be corrected and the spill remediated.
1939228024 2004-10-20 Production Wells No Violations Status check inspection - no violations at this time.
1955441408 2015-04-17 UrbanProduction Wells No Violations I inspected this well on 4/17/2015. The access road was graveled and offered access to the tank battery. The tank battery consisted of a 100 barrel oil tank, 50 barrel poly brine tank and a horizontal mechanical separator with orifice gas meter. The tank battery was fenced, locked and surrounded by a earthen dike. All piping and fittings were leak free. The required I D signage was in place. The well is operated as a pumping well with a natural gas motor. The well is located in a hay field and does not have a definite access road. At the wellhead pile ( 1.5X 1.5 ) of paraffin, drained out of the bleeding valve, was laying on the ground. I spoke with George Strawn ( Everfloe Eastern ) and asked for it to be removed.
36770624 2002-10-18 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1620647821 US-OH-115927 2002-10-20 Well operation causing pollution and contamination

For data sources see[9]

References