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34-153-22538

Well Details

Well ID: 34-153-22538
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: EKUS-DUNN UNIT
License Status: Plugged and Abandoned
License Date: 2016-12-08
Spud Date: 1991-01-03
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]]
Final Drill Date: 1991-01-11
Well Total Depth: 3945.00 ft
Configuration: Vertical
Latitude: 41.050000
Longitude: -81.530000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1988-10-31 1668 ENVIRONMENTAL EXP CO GeoDate 10/31/88
Oil and Gas 1988-10-31 Issued Date 10/31/88 Expired Date 10/31/89 Acres 0020716 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1989-11-22 1668 ENVIRONMENTAL EXP CO GeoDate 11/22/89
Oil and Gas 1989-11-22 Issued Date 11/22/89 Expired Date 11/22/90 Acres 0020716 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1990-12-17 1668 ENVIRONMENTAL EXP CO GeoDate 12/17/90
Oil and Gas 1990-12-17 Issued Date 12/17/90 Expired Date 12/17/91 Acres 0020716 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 03945 Proposed Drill Depth 03945
Original Spud 1991-01-03 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Completed 1991-01-11 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Reached Total Depth 1991-01-11 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Completion Report Received 1991-04-11 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Change of Owner 1999-10-14 Operator changed from 1668, ENVIRONMENTAL EXP CO to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2016-12-08 Proposed Formations:CLINTON GROUP, Issued Date:12/8/2016, Expired Date:12/8/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-01-11 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Record Last Modified 2017-03-29 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Construction Permit Expires 2018-12-08 RI 11-25-89, RI 12-22-90. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3722 3786 0
3722 3786 0
3722 3786 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 500 Gal 0 FRAC:WATER/SAND/ACID
ACID 0 500 Gal 0
H2O 0 94866 Gal 60000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1992 ENVIRONMENTAL EXP CO 14926.00 82.00 365
1993 ENVIRONMENTAL EXP CO 20460.00 40.00 365
1994 ENVIRONMENTAL EXP CO 18580.00 107.00 365
1995 ENVIRONMENTAL EXP CO 18127.00 0.00 365
1996 ENVIRONMENTAL EXP CO 13085.00 84.00 365
1997 ENVIRONMENTAL EXP CO 13809.00 57.00 365
1998 ENVIRONMENTAL EXP CO 13478.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 2131.00 0.00 91
2000 EXCO - NORTH COAST ENERGY INC 10156.00 93.00 365
2001 EXCO - NORTH COAST ENERGY INC 9354.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 8474.00 106.00 365
2003 EXCO - NORTH COAST ENERGY INC 7350.00 0.00 365
2004 EXCO - NORTH COAST ENERGY INC 2573.00 0.00 365
2005 EXCO - NORTH COAST ENERGY INC 6223.00 82.00 365
2006 EXCO - NORTH COAST ENERGY INC 7601.00 91.00 365
2007 EXCO - NORTH COAST ENERGY INC 5923.00 0.00 365
2008 EXCO - NORTH COAST ENERGY INC 5405.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 3949.00 80.00 365
2010 ENERVEST OPERATING LLC 2927.00 51.00 365
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 1
2016 ENERVEST OPERATING LLC 0.00 0.00 2
2017 ENERVEST OPERATING LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1992 ENVIRONMENTAL EXP CO Brine 49969 365
1993 ENVIRONMENTAL EXP CO Brine 4497 365
1994 ENVIRONMENTAL EXP CO Brine 2625 365
1995 ENVIRONMENTAL EXP CO Brine 1920 365
1996 ENVIRONMENTAL EXP CO Brine 1688 365
1997 ENVIRONMENTAL EXP CO Brine 1525 365
1998 ENVIRONMENTAL EXP CO Brine 1564 365
1999 EXCO - NORTH COAST ENERGY INC Brine 91
2000 EXCO - NORTH COAST ENERGY INC Brine 1247 365
2001 EXCO - NORTH COAST ENERGY INC Brine 1412 365
2002 EXCO - NORTH COAST ENERGY INC Brine 1304 365
2003 EXCO - NORTH COAST ENERGY INC Brine 1276 365
2004 EXCO - NORTH COAST ENERGY INC Brine 864 365
2005 EXCO - NORTH COAST ENERGY INC Brine 1372 365
2006 EXCO - NORTH COAST ENERGY INC Brine 1134 365
2007 EXCO - NORTH COAST ENERGY INC Brine 1118 365
2008 EXCO - NORTH COAST ENERGY INC Brine 1014 366
2009 ENERVEST OPERATING LLC Brine 0 92
2010 ENERVEST OPERATING LLC Brine 303 365
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 1
2016 ENERVEST OPERATING LLC Brine 0 2
2017 ENERVEST OPERATING LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-89263969 2016-11-2 0:00: UP No Violations
0089263969 2016-11-02 UrbanProduction Wells No Violations I received a request to field check the Ekus - Dunn # 1 from Craig Kowalski of HzW Environmental Consultants, LLC, Akron, OH. Mr. Kowalski was conducting Phase Two environmental assessment for a purchaser of the property when he located this well. The Divisions Well Locator map did not spot any wells on the property. The well was misplotted, approximately 9900 to the west. The well and tank battery were located in a auto recycling facility located at 663 Kenmore Blvd. Access was gained through the yard for both. The well last reported oil and gas volumes in 2010. There were not any outstanding Notices of Violations or Compliance Notices regarding the well. The well was drilled in 1991. The well was operated as a pumping well with 2.375 tubing and rods inside 4.5 production casing. The well was not operational as the pumping unit had been removed. Remnants of the stone pad and fencing panels remained. No leaks were identified during this inspection. The valves on the well head were in the position. There was minor ground contamination associated with a pumping well operation. Gauges on the well head were not operational. The tank battery was located approximately 80 north of the well head and consisted of one (1) 210 barrel oil tank, one (1) drip bottle, one (1) gas meter and associated two (2) inch piping. There was not a separator present. The tank battery was surrounded with a chain link fence, but was not locked. The I.D. sign was not legible. The yard operator has partially fulled the tank battery fencing with used auto gas tanks, restricting complete access. The vegetation inside the tank battery was overgrown and impeded a complete visual inspection. I did not identify any releases of oil and / or brine around the tank. I spoke with Mr. Leonard Ekus, owner, who supplied a check ( Delayed Rental payment ) with the well name and identified the Operator ( Enervest Operating LLC ). I spoke with Tim McConaha ( Enervest Operating ) to inquire about the well. Mr. M
1390265780 2016-11-07 UrbanProduction Wells No Violations I met with Tim McConaha ( Enervest Operating ) to conduct a pre-plugging evaluation to generate a plugging protocol for the well. The 2.375 tubing was opened, through a one (1) inch bleed off line, to the atmosphere for 10 minutes. No pressure or fluid flow was observed. The 4.5 production casing was opened through a quarter inch needle valve and a flow of brackish fluid( 618 ppm Cl ) was observed. I extrapolated this flow to be one (1) gallon of fluid every 32 minutes. The 8.625 surface casing head was exposed and opened with an unmeasurable pressure which blew down to 0 psi in less than one (1) minute. No fluid flow was observed from the 8.625 X 4.5 annulus. I requested that Enervest Operating submit a plugging scheme for DOGRMs review and approval. No violations identified during this inspection.

For data sources see[9]

References