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34-153-23096

Well Details

Well ID: 34-153-23096
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: DOMINION EAST OHIO
Well Pad ID:
Farm/Lease Name: COLLOCA UNIT
License Status: Storage Well
License Date: 2014-03-04
Spud Date: 2009-09-14
Spud Drilling Contractor: WHIPSTOCK OHIO DRILLING
Final Drill Date: 2009-09-28
Well Total Depth: 4105.00 ft
Configuration: Vertical
Latitude: 40.940000
Longitude: -81.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2009-09-03 Proposed Formations:CLINTON, Issued Date:9/3/2009, Expired Date:9/3/2010 6:00:00 AM, Drilling unit acres:60, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2009-09-28
Completion Report Received 2009-11-17
Change of Owner 2010-04-30 Operator changed from 8321, DOMINION EXPL& PROD INC to 8632, DOMINION FIELD SERVICES INC
Change of Owner 2014-02-20 Operator changed from 8632, DOMINION FIELD SERVICES INC to 240, DOMINION EAST OHIO
APP 2014-03-03 Proposed Formations:CLINTON, Issued Date:3/3/2014, Expired Date:3/2/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SO, Proposed Well Class:
APP 2014-03-04 Proposed Formations:CLINTON, Issued Date:3/4/2014, Expired Date:3/3/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SO, Proposed Well Class:
Construction Permit Expires 2015-03-04
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2010-02-03 3897 3964 22
3897 3964 22
3897 3964 22

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 1752 Bbl 61135 574,341 SCF NITROGEN ASSIST

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 DOMINION EXPL& PROD INC 1019.00 440.00 59
2010 DOMINION FIELD SERVICES INC 8443.00 1461.00 365
2011 DOMINION EAST OHIO 13241.00 818.00 365
2012 DOMINION FIELD SERVICES INC 9717.00 628.00 366
2013 DOMINION FIELD SERVICES INC 6869.00 544.00 355

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 DOMINION EXPL& PROD INC Brine 51 59
2010 DOMINION FIELD SERVICES INC Brine 371 365
2011 DOMINION EAST OHIO Brine 0 365
2012 DOMINION FIELD SERVICES INC Brine 201 366
2013 DOMINION FIELD SERVICES INC Brine 310 355

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1187439220 2009-9-9 0:00:0 DD No Violations
-1475456531 2009-9-21 0:00: DD No Violations
-1491836148 2009-9-14 0:00: DD No Violations
-1989454553 2020-3-31 0:00: SO No Violations 0.50
-2065177295 2019-1-16 0:00: SO No Violations 0.50
-784993064 2009-9-17 0:00: DD No Violations
0039802026 2009-09-22 Drill / Deepen / Reopen No Violations Whipstock continued to drill the Salina without establishing circulation. TD of 3356 was reached and Whipstock laid down the drillstring in order to run the 7 casing.
0570623632 2009-10-01 Drill / Deepen / Reopen No Violations Whipstock Drilling has moved off the location and the drilling pits are being pumped down. The pits are fenced, lined and in good condition.
0671429852 2018-02-15 Storage Well No Violations I did a status check inspection for this storage well. The well is equipped with a plunger-lift system. The diked tank battery consists of two steel tanks, a plastic brine tank, a horizontal separator, a vertical separator and a meter. The well and tank battery are fenced in with locked gates. The well is legibly identified. No compliance issues are cited at this time.
0784993064 2009-09-17 Drill / Deepen / Reopen No Violations Whipstock first encountered water at 2657 in the Oriskany. The water volume was contolled with the addition of soap. Additional water was reported at 2892 which forced Whipstock to convert from air to fluid drilling.
0796735971 2009-10-07 Drill / Deepen / Reopen No Violations Daily Excavating and ChemTech are on site to solidify the drilling pits.
1093192274 2009-09-11 Drill / Deepen / Reopen No Violations The drilling location and the lease road have been built. The rig is scheduled to move on location on 9/14.
1187439220 2009-09-09 Drill / Deepen / Reopen No Violations Daily Excavating was on site to start building the lease road and the location. No violations at this time.
1254183271 2009-09-18 Drill / Deepen / Reopen No Violations Whipstock Drilling encountered the top of the Big Lime at 2392 while drilling with air. At a depth of 2657 they had a show of water from the Oriskany which caused them to start soaping. At 2892 the water volume forced a conversion to fluid drilling before brine started flowing to surface. The weight of the brine was measured at 9.2 ppg. Whipstock mixed a pill of gel and cottonseed hulls in an attempt to control brine flow and loss. The pill was unsuccessful and Dominion decided to pump a cement plug to shut off the zone. Petroset mixed and pumped a 300 sack plug of Class A cement without circulating during the job. The plug was down at 06:15 am on 9/18. Whipstock waited 24 hours before going back to drilling.
1293778904 2014-12-26 UrbanProduction Wells No Violations I was on location to conduct a status check of this well. The well is of plunger lift construction. The tank battery consists of two 140 BBL production tanks, a mechanical separator and a 1500 gallon poly brine tank. The valves at the wellhead were open. The low pressure relief valve, spark arrestor and charcoal filter were installed on one of the 140 BBL production tanks. The tank battery was diked. The fencing around the wellhead and tank battery is an 8 foot high chain link fence and topped with three strands of barbed wire. The man doors to the tank battery and well were locked. The well is properly identified with a clear, legibly marked well identification sign. The lease road is stable and drivable. No violations found.
1422512417 2017-01-26 Storage Well No Violations At the time of this inspection, the well was equipped with a plunger lift assembly and the valves on the wellhead were closed and locked. The well was fenced and locked. The tank battery still contained production equipment and consisted of two 100 BBL production tanks, one 50 BBL poly brine tank, and a mechanical separator. The valves on the separator were closed. The tank battery was diked and fenced with a locked man door. The fence had been damaged by a downed tree on the northwest side and the tree debris has been removed but fence still needs repaired. The proper, legible signage was located at the tank battery. Lease access was stable. I contacted Dominion East Ohio about repairing the fence around the tank battery.
1475456531 2009-09-21 Drill / Deepen / Reopen No Violations After waiting on the second cement plug, Whipstock ran the 7-7/8 drillstring back in the hole and tagged the cement at 1953. For the next 24 hours, Whipstock drilled cement back to a depth of 2892. Whipstock continued drilling the Salina to a depth of 2975 where circulation was lost again. Dominion decided to continue drilling without circulation through the salt intervals before setting an intermediate string of 7 casing. Fluid loss to this point totaled nearly 4000 bbl.
1491836148 2009-09-14 Drill / Deepen / Reopen No Violations Whipstock Drilling has spudded the well and is drilling conductor hole. Surface casing should be ready to cement in the morning. The working pit has been dug and lined. The blow pit will be dug in the morning.
1656125621 2010-06-23 Preliminary Restoration No Violations Preliminary restoration is approved.
1672153618 2009-09-28 Drill / Deepen / Reopen No Violations Whipstock Drilling has reached TD and is starting to lay down drill pipe. The intermediate casing job has apparently been successful in containing the water flow from the Salina Group.
1767022051 2009-09-23 Drill / Deepen / Reopen No Violations After waiting 12 hours for the 7 cement, Appalachian Well Surveys ran a cement bond log. The logging tool set down at 3233 and found the top of cement on the backside of the 7 casing at 2998. This placed the top of the cement near the base of the loss circulation zone. In order to place cement above this zone, Appalachian perforated the 7 with 8 shots from 2530 to 2532. Petroset mixed and displaced 150 sacks of Class A cement with 3% calcium chloride. The plug was down at 12:50 am on 9/24 and the well was shut in for 8 hours.
1776146716 2009-09-19 Drill / Deepen / Reopen No Violations After waiting on cement spotted on 9/18, Whipstock ran the 7-7/8 drillstring back into the hole. They did not encounter any of the cement but there was a diminution in the flow volume. Dominion decided to place a second cement plug across the same interval. On 9/19, Petroset pumped another 300 sack plug of Class A cement this time with 2% calcium chloride added. Circulation was maintained throughout the cement mixing and displacement. The plug down was at 14:40 on 9/19.
2065177295 2019-01-16 Storage Well No Violations My inspection found the well is equipped with a plunger-lift system. The diked tank battery consists of two steel tanks, a plastic brine tank, a meter run, a vertical and horizontal separator. The well is legibly identified. No compliance issues are cited at this time.
2079933940 2009-11-24 Production Wells No Violations The well is in production and the required fences and identification are posted. The affected areas have been graded, seeded and mulched. Preliminary restoration will be approved as soon as the vegetation has established.
39802026 2009-9-22 0:00: DD No Violations
570623632 2009-10-1 0:00: DD No Violations
671429852 2018-2-15 0:00: SO No Violations 0.50
796735971 2009-10-7 0:00: DD No Violations

For data sources see[9]

References