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34-153-23122

Well Details

Well ID: 34-153-23122
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: DOMINION FIELD SERVICES INC
Well Pad ID:
Farm/Lease Name: DEO UNIT
License Status: Lost Hole
License Date: 2010-10-08
Spud Date: 2011-02-18
Spud Drilling Contractor: WILDCAT DRILLING
Final Drill Date: 2011-02-21
Well Total Depth:
Configuration: Directional
Latitude: 40.950000
Longitude: -81.640000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2010-10-08 Proposed Formations:CLINTON, Issued Date:10/8/2010, Expired Date:10/7/2012 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2011-02-21 HOLE DEVIATED ~ 4 DEGREES EAST @ ~ 1100 '. WILL P&A AND SKID TO DRILL 3-D-
Reached Total Depth 2011-02-21 HOLE DEVIATED ~ 4 DEGREES EAST @ ~ 1100 '. WILL P&A AND SKID TO DRILL 3-D-
Construction Permit Expires 2011-10-08 HOLE DEVIATED ~ 4 DEGREES EAST @ ~ 1100 '. WILL P&A AND SKID TO DRILL 3-D-
Record Last Modified 2015-02-09 HOLE DEVIATED ~ 4 DEGREES EAST @ ~ 1100 '. WILL P&A AND SKID TO DRILL 3-D-

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1298909530 2011-02-22 Plug / Plug Back No Violations Dominion lost the hole at 1130 feet and decided to plug back to surface and skid the rig. The hole deviated approximately four degrees to the east. The angle was managable but the direction was not. On 2/21, Wildcat and Petroset plugged the well from 890 feet to surface using open ended drill pipe. The rathole and mousehole were also plugged prior to moving the rig.

For data sources see[3]

References