X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-157-21833

Well Details

Well ID: 34-157-21833
Loading map...
Country: United States
State: Ohio
County: Tuscarawas
Municipality: Sugar Creek Township
Operator Name: RIVERSIDE PETROLEUM & PROD.
Well Pad ID:
Farm/Lease Name: DEETZ UNIT
License Status: Final Restoration
License Date: 2017-10-11
Spud Date: 1973-04-23
Spud Drilling Contractor:
Final Drill Date: 1973-12-03
Well Total Depth:
Configuration: Vertical
Latitude: 40.500000
Longitude: -81.610000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1972-12-15 139 MB OPERATING CO INC GeoDate 12/15/72
Original Spud 1973-04-23 REV. LOC. 4-11-73 GMM UPDATED PLUG STATUS PER PLUG REPORT
Completed 1973-12-03 REV. LOC. 4-11-73 GMM UPDATED PLUG STATUS PER PLUG REPORT
Reached Total Depth 1973-12-03 REV. LOC. 4-11-73 GMM UPDATED PLUG STATUS PER PLUG REPORT
APP 1997-11-12 Proposed Formations:CLINTON, Issued Date:11/12/97, Expired Date:11/12/98 6:00:00 AM, Drilling unit acres:87.17, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2000-06-30 Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC
Change of Owner 2001-04-03 Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 6868, RIVERSIDE PETROLEUM & PROD.
APP 2017-10-11 Proposed Formations:CLINTON, Issued Date:10/11/2017, Expired Date:10/11/2019 12:00:00 PM, Drilling unit acres:81.17, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-04-14 REV. LOC. 4-11-73 GMM UPDATED PLUG STATUS PER PLUG REPORT
Record Last Modified 2018-07-11 REV. LOC. 4-11-73 GMM UPDATED PLUG STATUS PER PLUG REPORT
Construction Permit Expires 2019-10-11 REV. LOC. 4-11-73 GMM UPDATED PLUG STATUS PER PLUG REPORT

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4328 4398 0
4328 4398 0
4328 4398 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 88000 Gal 0 AVG. PUMP RATE 66.12 BPM; AVG. PRESS. W/SD. 2300#; HHP USED 3462.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC 2010.00 0.00 365
1985 RESOURCE AMERICA INC 1704.00 0.00 365
1987 RESOURCE AMERICA INC 0.00 0.00 365
1988 MB OPERATING CO INC 0.00 0.00 366
1989 MB OPERATING CO INC 0.00 0.00 365
1990 MB OPERATING CO INC 0.00 0.00 365
1992 MB OPERATING CO INC 0.00 0.00 366
1993 MB OPERATING CO INC 0.00 0.00 365
1994 MB OPERATING CO INC 0.00 0.00 365
1995 MB OPERATING CO INC 0.00 0.00 365
1996 MB OPERATING CO INC 0.00 0.00 366
1997 MB OPERATING CO INC 0.00 0.00 365
1998 MB OPERATING CO INC 0.00 0.00 365
1999 MB OPERATING CO INC 0.00 0.00 273
2001 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2002 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2003 RIVERSIDE PETROLEUM & PROD. 125.00 0.00 360
2004 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2005 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2006 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2007 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2008 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2009 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2010 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2011 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2012 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2013 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2014 RIVERSIDE PETROLEUM & PROD. 0.00 40.00 180
2015 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2016 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0
2017 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 365
2018 RIVERSIDE PETROLEUM & PROD. 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC Brine 0 365
1985 RESOURCE AMERICA INC Brine 0 365
1987 RESOURCE AMERICA INC Brine 0 365
1988 MB OPERATING CO INC Brine 0 366
1989 MB OPERATING CO INC Brine 0 365
1990 MB OPERATING CO INC Brine 0 365
1992 MB OPERATING CO INC Brine 0 366
1993 MB OPERATING CO INC Brine 0 365
1994 MB OPERATING CO INC Brine 0 365
1995 MB OPERATING CO INC Brine 0 365
1996 MB OPERATING CO INC Brine 0 366
1997 MB OPERATING CO INC Brine 0 365
1998 MB OPERATING CO INC Brine 0 365
1999 MB OPERATING CO INC Brine 0 273
2001 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2002 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2003 RIVERSIDE PETROLEUM & PROD. Brine 0 360
2004 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2005 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2006 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2007 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2008 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2009 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2010 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2011 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2012 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2013 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2014 RIVERSIDE PETROLEUM & PROD. Brine 6 180
2015 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2016 RIVERSIDE PETROLEUM & PROD. Brine 0 0
2017 RIVERSIDE PETROLEUM & PROD. Brine 0 365
2018 RIVERSIDE PETROLEUM & PROD. Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1486283651 2018-4-11 0:00: PB No Violations 3.80
-1554865694 2018-4-12 0:00: PB No Violations 5.60
-2075645312 2018-4-9 0:00:0 PB No Violations 1.00
-23320709 2017-7-26 0:00: PW No Violations 0.70
-777673038 2018-4-16 0:00: PB No Violations 6.20
0023320709 2017-07-26 Production Wells No Violations
0412349256 2018-04-18 Plug / Plug Back No Violations Upon my arrival on location, I witnessed the cement plug had settled 10 inches below the top of 8.625 inch diameter casing. The cement had a flat and hard finish, with no bubbles present. I then called ODNR Inspector Randy Akins to confirm what I witnessed, and he told me to give Riverside Petroleum the go ahead to back fill and reclaim location. They had already started to pump the pit out and dispose of the excess pit liner. Another inspection will be in order later.
0777673038 2018-04-16 Plug / Plug Back No Violations Upon arriving on location, I was accompanied by Inspector Jeff Adams. The rig crew tagged the cement top at 780 feet. 10 bbl. of lost circulation material was pumped ahead, and was chased with 25 bbl. of fresh and circulation was established. A 200 foot plug was set by using Class A cement and displaced with fresh water. The well did circulate, but in the process of pump the cement the well lost circulation. The tubing was then remove from the tubing and we shut down for a period of 2.5 hours. We then established circulation and pumped 60 sack of class A cement plug, and half way through we then lost circulation and shut down for the night.
0839654321 2018-04-09 Plug / Plug Back No Violations On the day of inspection I accompanied ODNR Inspector Randy Akins. See his report for details.
1486283651 2018-04-11 Plug / Plug Back No Violations Upon arrival on location I was accompanied by Inspector Jeff Adams. We found the rig getting to plug and abandon well. A wireline was run in the wellbore to a depth of 4315. They were then running 1 1/2 tubing into wellbore to spot the bottom cement plug.
1523552660 2018-04-11 Plug / Plug Back No Violations On the day of inspection I accompanied ODNR Inspector Randy Akins. See his report for details.
1523903430 2018-04-16 Plug / Plug Back No Violations On the day of inspection I accompanied ODNR Inspector Randy Akins. See his report for details.
1523972373 2018-04-17 Orphan No Violations Upon arriving on location, I was accompanied by Inspector Jeff Adams. The rig crew tagged the top of the cement at 45 feet. 1 1/2 yard of 9 sack grout was used to top of the well.
1523974449 2018-04-17 Plug / Plug Back No Violations On the day of inspection I accompanied ODNR Inspector Randy Akins. See his report for details.
1527163516 2018-05-24 Final Restoration No Violations On the day of inspection, I found that the final restoration inspection has been completed. The site passed final restoration according to ORC 1509.072 (B).
1554865694 2018-04-12 Plug / Plug Back No Violations On the day of inspection I accompanied ODNR Inspector Randy Akins. See his report for details.
2075645312 2018-04-09 Plug / Plug Back No Violations Arrived on location I was accompanied by Inspector Jeff Adams. The service rig has been moved on location. Inspector Jeff and I discussed where we thought the plugs should be set.
412349256 2018-4-18 0:00: PB No Violations 1.00
839654321 2018-4-9 0:00:0 PB No Violations 1.00

For data sources see[9]

References