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34-157-24913

Well Details

Well ID: 34-157-24913
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Oxford Township
Operator Name: POORBOY EXPLORATION LLC
Well Pad ID:
Farm/Lease Name: GEORGE ROGER W & ANGELINE W
License Status: Producing
License Date: 1994-01-12
Spud Date: 1994-02-14
Spud Drilling Contractor: UNGER DRILLING
Final Drill Date: 1994-03-05
Well Total Depth: 7178.00 ft
Configuration: Vertical
Latitude: 40.270000
Longitude: -81.560000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1994-01-12 2960 TUCO PARTNERSHIP GeoDate 1/12/94
Oil and Gas 1994-01-12 Issued Date 1/12/94 Expired Date Acres 0202569 Tool Type RTAF Proposed Formation CLINTON thru RR Proposed Depth Proposed Drill Depth
Original Spud 1994-02-14
Completed 1994-03-05
Plugged Back 1994-03-05
Reached Total Depth 1994-03-05
Completion Report Received 1994-09-16
Construction Permit Expires 1995-01-12
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4570 4667 0
4570 4667 0
2006-09-11 4571 4667 49
4571 4667 49
4570 4667 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 0 FRAC...WATER & SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 TUCO OPERATING PARTNERS,LLC 4332.00 75.00 365
2009 TUCO OPERATING PARTNERS,LLC 3813.00 23.00 365
2010 TUCO OPERATING PARTNERS,LLC 3972.00 0.00 365
2011 TUCO OPERATING PARTNERS,LLC 4147.00 5.00 365
2012 TUCO OPERATING PARTNERS,LLC 4325.00 5.00 366
2013 ENDEAVOR OHIO LLC 2100.00 19.00 365
2016 POORBOY EXPLORATION LLC 271.00 0.00 0
2017 POORBOY EXPLORATION LLC 933.00 0.00 240
2018 POORBOY EXPLORATION LLC 898.00 0.00 240

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 TUCO OPERATING PARTNERS,LLC Brine 15 365
2009 TUCO OPERATING PARTNERS,LLC Brine 0 365
2010 TUCO OPERATING PARTNERS,LLC Brine 0 365
2011 TUCO OPERATING PARTNERS,LLC Brine 0 365
2012 TUCO OPERATING PARTNERS,LLC Brine 37 366
2013 ENDEAVOR OHIO LLC Brine 32 365
2016 POORBOY EXPLORATION LLC Brine 0 0
2017 POORBOY EXPLORATION LLC Brine 0 240
2018 POORBOY EXPLORATION LLC Brine 0 240

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1391305255 2015-4-22 0:00: PW No Violations 1.00
-1937255337 2018-6-1 0:00:0 PW No Violations 0.30
-2090781573 2016-3-22 0:00: PW No Violations 1.50
-605131730 2016-6-24 0:00: PW No Violations 1.00
-821544026 2015-4-29 0:00: PW No Violations 1.50
0605131730 2016-06-24 Production Wells No Violations
0821544026 2015-04-29 Production Wells No Violations On the day of my inspection I found a 8 X 4 wellhead and a 4 X 1.5 inch wellhead, operated by a plunger lift system. The tank battery is made up of two 100 bbl tank, a horizontal separator, and a recording gauge. All in an earthen dike. The tank is not properly identified, and the production reporting is up to date. This well is being operated by an unregustered owner. The last year of reported production was 2012 by Endevor of Ohio. I belleive that Poorboy is operating the well. I will advise them to stop production until they become the owner of record.
1391305255 2015-04-22 Production Wells No Violations On the date of inspection I am following up on a Compliance Notice issued on 10-31-14 for a failure to legibly identify well. I found production equipment to include two 100bbl tanks and a horizontal separator within an earthen dike. The well is equipped with a gas plunger lift system, 1.5 inch tubing, 4.5 inch casing, and 8.625 inch casing. The tubing valve and one casing valve are in open position. 2012 was the last year that production was reported. There is no identification in place at the well or the tank battery. There is a 3 foot by 3 foot area within the dike that is contaminated with oil. I will be working with ODNR Inspector Randy Akins on determining the ownership of the well to have the issues addressed.. The current listed owner is no longer in business.
1414689329 2014-10-30 Production Wells Violations Noted On the day of my inspection I found a well with a 8 X 4 inch wellhead and a 4 X 1 1/2 wellhead, operated with a plunger lift system. The valves were in the open position. The tank battery was made up of two 100 bbl tanks, and a horizontal separator in an earthen dike. The tanks are not identified, I have placed a call to Tuco at 1:17pm and left a message to return my call. The tank battery is located approximately 100 feet away from a public highway.
1449667143 2015-12-09 Production Wells No Violations On the day of my inspection I found that there is no change in the status of ownership. The owner of record is TUCO Partnership, but the well has been operated by Poor Boy.
1478617275 2016-11-08 Production Wells No Violations
1508934769 2017-10-25 Production Wells No Violations On the day of my inspection I found an 8 5/8 inch diameter casing, a 4 1/2 inch diameter casing, a 1 1/2 inch diameter tubing operated by a plunger lift system. The valves are in the open position. The production equipment is made up of two 100 bbl. tanks and a horizontal separator, and a recording gauge. The outlet valve on the separator is in the open position. The tanks are properly identified. Ownership has not been cleared up, but Poor Boy is producing the well.
1556039053 2019-04-23 Production Wells No Violations This inspection was a follow up to a compliance notice number 1414689329, issued on 10/30/14 by ODNR Inspector Randy Akins for no identification. I witnessed the well was equipped 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, and a plunger lift system. The valves on the tubing and casing were open. Production equipment included two steel 100 barrel tanks, a horizonal separator, and chart recorder with an 2 by 1.250 inch orifice plate within an earthen dike. The production report was up to date and identification was present. The ownership of the well has not been cleared up from Tuco Partnership to Poor Boy Exploration. Poorboy Exploration has been operating the well.
1580134696 2020-1-27 0:00: PW No Violations 0.40
1937255337 2018-06-01 Production Wells No Violations Upon arrival on location, I witnessed the well was equipped 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, and a plunger lift system. The valves on the tubing and casing were open. Production equipment included two steel 100 barrel tanks, a horizonal separator, and chart recorder with an 2 by 1.250 inch orifice plate within an earthen dike. The production report was up to date and proper identification was present. The ownership of the well has not been cleared up, but Poor Boy Exploration has been operating the well.
2090781573 2016-03-22 Production Wells No Violations On the day of my inspection I found the well has been put back into production. The well has been idle do to a question of ownership. Poor Boy Exploration has alleged that they are the owner of the well, and are producing the well. I contacted David Bonar with Poor Boy Exploration and advised him that the well needs to be shut in. In the State of Ohio records Tuco Partnership is still the owner of record. I will contact bonding and surety to see if this matter has been resolved.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1414689329 US-OH-112188 2014-11-05 Failure to legibly identify well

For data sources see[9]

References