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34-169-24878

Well Details

Well ID: 34-169-24878
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Country: United States
State: Ohio
County: Wayne
Municipality: Milton Township
Operator Name: MORTON SALT INC
Well Pad ID:
Farm/Lease Name: MORTON SALT {SMP #4}
License Status: Final Restoration
License Date: 2011-12-14
Spud Date: 1991-12-16
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1991-12-21
Well Total Depth: 2590.00 ft
Configuration: Vertical
Latitude: 40.950000
Longitude: -81.800000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1991-10-08 3509 MORTON SALT/MORTON INTL GeoDate 10/8/91
Solution Mining 1991-10-08 Issued Date 10/8/91 Expired Date 10/7/92 Acres 0000000 Tool Type RTAF Proposed Formation SALINA Proposed Depth 02547 Proposed Drill Depth 02547
Original Spud 1991-12-16
Completed 1991-12-21
Reached Total Depth 1991-12-21
Completion Report Received 1992-01-28
Annulus Pressure Monitoring Approved 1996-08-07
Last Compliance Report 2006-05-23
Change of Owner 2010-11-29 Operator changed from 3509, MORTON SALT INC to 8736, MORTON SALT INC
APP 2011-12-14 Proposed Formations:SALINA, Issued Date:12/14/2011, Expired Date:12/13/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SWIW
Plugged/Abandoned 2013-03-21
Construction Permit Expires 2013-12-13
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1999-09-13 2496 2559 0
2496 2559 0
2496 2559 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NOT TREATED

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1576978632 2003-12-9 0:00: SM No Violations
0785163438 2013-03-21 Plug / Plug Back No Violations 2-3/8 EUE tubing was run in this well to the mechanical bridge plug at 2102. Universal Cementing set 5 cement plugs in this well through tubing this date. This well was plugged solid with cement from bottom to top. The plug did not drop back. See the plugging record for details.
1148414523 2006-05-19 Solution Mining Project No Violations The 5 Year MIT was completed for this well using the #32 well (PN 4687) as the reference well. The following table summarizes the results of this test. The well passed with a net change of 0.013 psi/hr.

TIME TEST PRESS. REF.PRESS. DIFF. TIME TEST PRESS. REF.PRESS. DIFF. 0700 264.971 64.017 200.954 1200 263.698 62.723 200.975 0800 264.725 63.755 200.970 1300 263.452 62.503 200.949 0900 264.406 63.455 200.951 1400 263.417 62.324 201.093 1000 264.108 63.114 200.994 1500 263.159 62.106 200.053 1100 263.896 62.315 201.581

1210i28571 2002-03-27 Solution Mining Project No Violations Well appears ok. Accompanied by Tom T. & Dave H.
1210i2857184 2002-3-27 0:00: SM No Violations
1348570414 2012-09-24 Solution Mining Project No Violations Identification in place. No problems noted.
1363953793 2013-03-20 Plug / Plug Back No Violations An 8 mechanical bridge plug was run in this well and set at 2102. A subsequest pressure test barely failed. The well will be plugged out.
1369053707 2013-05-20 Final Restoration No Violations Appears to be in compliance.
1576978632 2003-12-09 Solution Mining Project No Violations CHECKED ID - OK
785163438 2013-3-21 0:00: PB No Violations

For data sources see[5]

References