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34-169-25133

Well Details

Well ID: 34-169-25133
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Country: United States
State: Ohio
County: Wayne
Municipality: Milton Township
Operator Name: MORTON SALT INC
Well Pad ID:
Farm/Lease Name: MORTON SALT (SMP #4)
License Status: Final Restoration
License Date: 2012-12-17
Spud Date: 1996-12-11
Spud Drilling Contractor: IPSCO
Final Drill Date: 1996-12-21
Well Total Depth: 2600.00 ft
Configuration: Vertical
Latitude: 40.950000
Longitude: -81.800000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1996-10-09 3509 MORTON SALT/MORTON INTL GeoDate 10/9/96
Solution Mining 1996-10-09 Issued Date 10/9/96 Expired Date 10/9/97 Acres 0000000 Tool Type RTAF Proposed Formation SALINA Proposed Depth 02600 Proposed Drill Depth 02600
Original Spud 1996-12-11
Completed 1996-12-21
Reached Total Depth 1996-12-21
Annulus Pressure Monitoring Approved 1997-01-07
Completion Report Received 1997-01-09
Last Compliance Report 2008-03-10
Change of Owner 2010-11-29 Operator changed from 3509, MORTON SALT INC to 8736, MORTON SALT INC
APP 2012-12-17 Proposed Formations:SALINA, Issued Date:12/17/2012, Expired Date:12/17/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP
Plugged/Abandoned 2014-10-28
Construction Permit Expires 2014-12-17
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1999-09-13 2475 2545 0
2475 2545 0
2475 2545 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NONE

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1020914773 2008-2-28 0:00: SM No Violations 2.50
-1299858926 2014-10-29 0:00 PB No Violations 0.50
-1468029042 2008-2-5 0:00:0 SM No Violations 0.70
-1596626081 2008-1-28 0:00: SM No Violations 0.70
-1711648246 2014-5-28 0:00: SM No Violations 0.50
-2019213836 2014-10-27 0:00 PB No Violations 6.00
-787821277 2007-9-20 0:00: SM No Violations 9.50
-851657938 2008-1-31 0:00: SM No Violations 8.50
-906380732 2014-10-29 0:00 SM No Violations 0.50
0029276107 2002-05-22 Solution Mining Project No Violations Conduct M.I.T. for 5 year review .Test passed
0064934040 2008-03-13 Solution Mining Project No Violations Test M.I.T. Test continued from from the last test with all fluids remaining static until test was complete.
0066059618 2007-09-20 Solution Mining Project No Violations Arrive today for MIT and after 7 hrs test has failed .
0077003289 2007-10-10 Solution Mining Project No Violations Check to see if well is being worked on and found that nothing has been done.Well needs tested for leaks.
0453191907 2008-03-06 Solution Mining Project No Violations Check on site and found test is to continue on Friday because interface is holding.
0786202740 2008-03-07 Solution Mining Project No Violations Test M.I.T. And test failed .
0787821277 2007-09-20 Solution Mining Project No Violations Arrive for test today and after 7 hours before 8th reading test was stopped as it was going to fail.
0851657938 2008-01-31 Solution Mining Project No Violations Arrive today for M.I.T on well using tubing on 40 for reference .Test was stopped for equipment repairs and scheduled again on Monday or Tuesday.Casing on well had frozen and needed torch to begin test.Test would have failed if continued.
0906380732 2014-10-29 Solution Mining Project No Violations ID is in place and legible. No apparent problems at this time.
1020914773 2008-02-28 Solution Mining Project No Violations Chiefs order has been issued to shut well in.I checked today and had field operations meet on site and go over how the well is operating.The line on both sides are open to allow just enough fluid to circulate thru the annulus side of the valve to keep it from freezing.
1205165316 2008-03-07 Solution Mining Project No Violations Arrive today for test on well which has been issued a Chiefs order because the last two M.I.T. have failed.Prior to the test the cavern has been pumped up to 198.792 psi and ended at 6:30 am on the same day of the test.The well used to pressure up the cavern was # 41 Permit # 5292 - After the test has ended I checked the pressure on this same well and found it down to 120 psi.The well tested today # 40 was also the well used for Reference.I should have had # 41 as the Reference and should have had it with a meter on it so that I could have monitored the pressure prior ,during and end.Any future tests which need the cavern to remain pressured before the test will be monitored during and after.
1210i27571 2002-03-27 Solution Mining Project No Violations Well appears ok. Meter 516,933gal. Accompanied by Tom Tomastik and Dave Hodges.
1210i2757183 2002-3-27 0:00: SM No Violations
1299858926 2014-10-29 Plug / Plug Back No Violations Pit has been closed. Plug has remained within 12 inches of surface.
1321098962 2007-10-11 Solution Mining Project No Violations Check well today to see if work has been done to prepare well for M.I.T. and found nothing done.
1355223953 2014-10-22 Plug / Plug Back No Violations On location to discuss plugging procedure with rig crew and company representative.
1394121520 Solution Mining Project No Violations Well is shut in and will be plugged when weather breaks. No apparent problems at time of inspection.
1435585780 2015-06-29 Final Restoration No Violations Appears to meet all requirements for final restoration. FINAL RESTORATION IS APPROVED.
1468029042 2008-02-05 Solution Mining Project No Violations Check to see if anybody is working on well and found no equipment and nobody working on site today.
1537870786 2012-09-24 Solution Mining Project No Violations Identification in place. No problems noted.
1596626081 2008-01-28 Solution Mining Project No Violations Morton was to pump interface today but after waiting on water truck job was cancelled for today.rescheduled for Tuesday.
1711648246 2014-05-28 Solution Mining Project No Violations Well is currently shut in and on list to be plugged. No apparent problems at this time.
1779483389 2003-12-09 Solution Mining Project No Violations CHECKED ID - OK
1812776594 2008-02-26 Solution Mining Project No Violations This well has not passed its M.I.T. and was to be shut in.I checked the well and found that it has both sides open so fluid is entering and leaving well .Check pressure on found pressure on both sides of well .Contact Morton and advise that well needs to be shut in.
1873195974 2004-09-02 Solution Mining Project No Violations Check on repairs to wells or equipment and found nobody around today and there appears not have been any work done on well.
1936593854 2008-03-05 Solution Mining Project No Violations Met Ed Willsie on site and pump interface to depth.
2019213836 2014-10-27 Plug / Plug Back No Violations On location to set bottom plugs. See plug report for details.
29276107 2002-5-22 0:00: SM No Violations 8.20
453191907 2008-3-6 0:00:0 SM No Violations 2.00
64934040 2008-3-13 0:00: SM No Violations 11.50
66059618 2007-9-20 0:00: SM No Violations 8.50
77003289 2007-10-10 0:00 SM No Violations 0.70
786202740 2008-3-7 0:00:0 SM No Violations 12.00
iANGE00015 1997-08-01 Preliminary Restoration No Violations
iANGE000152 1997-8-1 0:00:0 PL No Violations

For data sources see[5]

References