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37-005-00586

Well Details

Well ID: 37-005-00586
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Redbank Township
Operator Name: EQT PROD CO
Well Pad ID:
Farm/Lease Name: R W SHICK 4
License Status: Plugged and Abandoned
Spud Date: 1954-11-22
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.940984
Longitude: -79.231960

For data sources see[1][2][3]

Well History

Date Event
1955-01-01 Newly Drilled
1955-05-09 Drilling Completion
2017-11-06 Begin Plugging
2017-12-22 Finished Plugging
2018-09-21 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1986 APOLLO GAS CO 1,286.00 364 0.00 0 0.00 0
1987 APOLLO GAS CO 1,272.00 363 0.00 0 0.00 0
1988 APOLLO GAS CO 1,228.00 348 0.00 0 0.00 0
1989 APOLLO GAS CO 1,492.00 371 0.00 0 0.00 0
1991 APOLLO GAS CO 1172.00 359 0.00 0 0.00 0
1997 CARNEGIE PROD CO 1000 365 0.00 0 0.00 0
1998 CARNEGIE PROD CO 649 365 0.00 0 0.00 0
1999 CARNEGIE PROD CO 850 365 0.00 0 0.00 0
2000 EQUITRANS INC 789 365 0.00 0 0.00 0
2001 EQUITABLE PROD EASTERN STATES EXPLORATION INC 240 365 0.00 0 0.00 0
2003 EQT PROD CO 653 365 0.00 0 0.00 0
2004 EQT PROD CO 262 366 0.00 0 0.00 0
2005 EQT PROD CO 48 92 0 92 0.00 0
2006 EQT PROD CO 0.00 0 0.00 0 0.00 0
2007 EQT PROD CO 0.00 0 0.00 0 0.00 0
2008 EQT PROD CO 0.00 0 0.00 0 0.00 0
2009 EQT PROD CO 0.00 0 0.00 0 0.00 0
2010 EQT PROD CO 0.00 0 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0
2012 EQT PROD CO 0.00 0 0.00 0 0.00 0
2013 EQT PROD CO 0.00 0 0.00 0 0.00 0
2014 EQT PROD CO 0.00 0 0.00 0 0.00 0
2015 EQT PROD CO 0.00 0 0.00 0 0.00 0
2016 EQT PROD CO 0.00 0 0.00 0 0.00 0
2017 EQT PROD CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
219416 Primary Facility 1997-08-29 Routine/Complete Inspection No Violations Noted GAS LEAK REPAIRED/PROD GAS
2673777 Primary Facility 2017-12-21 Plugging(Includes Plugged/Mined Through) No Violations Noted TD'd well @ 2900'. Set CIBP inside 3" and set a cement plug from 2900' to 2740'. Set next plug from 2740' to 2500'. Went back in and tagged cement top @ 2492'. Cut and tripped out 2488' of 3" pipe. Went back in and set down @ 1590' as the hole had collapsed. Attempted to clean hole out and get back down but could not. Cemented from 1590' up to 758' which is the bottom of the 8" pipe and the crew was waiting for the logging truck to arrive to run in and tag the cement top at the time of this inspection. A bond log will then be run and reviewed to determine the process required to finish plugging the well.

For data sources see[6]

References