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Well ID: 37-005-00586 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Redbank Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: | |
Farm/Lease Name: R W SHICK 4 | |
License Status: Plugged and Abandoned | |
Spud Date: 1954-11-22 | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.940984 | |
Longitude: -79.231960 |
Date | Event |
---|---|
1955-01-01 | Newly Drilled |
1955-05-09 | Drilling Completion |
2017-11-06 | Begin Plugging |
2017-12-22 | Finished Plugging |
2018-09-21 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1986 | APOLLO GAS CO | 1,286.00 | 364 | 0.00 | 0 | 0.00 | 0 |
1987 | APOLLO GAS CO | 1,272.00 | 363 | 0.00 | 0 | 0.00 | 0 |
1988 | APOLLO GAS CO | 1,228.00 | 348 | 0.00 | 0 | 0.00 | 0 |
1989 | APOLLO GAS CO | 1,492.00 | 371 | 0.00 | 0 | 0.00 | 0 |
1991 | APOLLO GAS CO | 1172.00 | 359 | 0.00 | 0 | 0.00 | 0 |
1997 | CARNEGIE PROD CO | 1000 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | CARNEGIE PROD CO | 649 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | CARNEGIE PROD CO | 850 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | EQUITRANS INC | 789 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | EQUITABLE PROD EASTERN STATES EXPLORATION INC | 240 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | EQT PROD CO | 653 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | EQT PROD CO | 262 | 366 | 0.00 | 0 | 0.00 | 0 |
2005 | EQT PROD CO | 48 | 92 | 0 | 92 | 0.00 | 0 |
2006 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
219416 | Primary Facility | 1997-08-29 | Routine/Complete Inspection | No Violations Noted | GAS LEAK REPAIRED/PROD GAS |
2673777 | Primary Facility | 2017-12-21 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | TD'd well @ 2900'. Set CIBP inside 3" and set a cement plug from 2900' to 2740'. Set next plug from 2740' to 2500'. Went back in and tagged cement top @ 2492'. Cut and tripped out 2488' of 3" pipe. Went back in and set down @ 1590' as the hole had collapsed. Attempted to clean hole out and get back down but could not. Cemented from 1590' up to 758' which is the bottom of the 8" pipe and the crew was waiting for the logging truck to arrive to run in and tag the cement top at the time of this inspection. A bond log will then be run and reviewed to determine the process required to finish plugging the well. |
For data sources see[6]