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37-005-20021

Well Details

Well ID: 37-005-20021
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Burrell Township
Operator Name: EQT PROD CO
Well Pad ID:
Farm/Lease Name: SCHAEFFER 3
License Status: Plugged and Abandoned
Spud Date: 1956-07-27
Permit Date: 1956-06-29
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.681383
Longitude: -79.428433

For data sources see[1][2][3]

Well History

Date Event
1956-07-27 Performed Spud Operation
1956-10-10 Drilling Completion
1957-01-01 NEWLY DRILLED
2018-10-01 Begin Plugging
2018-10-25 Finished Plugging
2019-02-27 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 ANCIENT SANDS INC 632.00 365 0.00 0 0.00 0
2000 ANCIENT SANDS INC 100 365 0.00 0 0.00 0
2001 ANCIENT SANDS INC 1029.2 320 0.00 0 0.00 0
2003 ANCIENT SANDS INC 0.00 0 0.00 0 0.00 0
2004 ANCIENT SANDS INC 658 365 0.00 0 0.00 0
2005 ANCIENT SANDS INC 632 365 0.00 0 0.00 0
2006 ANCIENT SANDS INC 0.00 0 0.00 0 0.00 0
2007 ANCIENT SANDS INC 0.00 0 0.00 0 0.00 0
2008 ANCIENT SANDS INC 0.00 0 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0
2012 EQT PROD CO 0.00 0 0.00 0 0.00 0
2013 EQT PROD CO 0.00 0 0.00 0 0.00 0
2014 EQT PROD CO 0.00 0 0.00 0 0.00 0
2015 EQT PROD CO 0.00 0 0.00 0 0.00 0
2016 EQT PROD CO 0.00 0 0.00 0 0.00 0
2017 EQT PROD CO 0.00 0 0.00 0 0.00 0
2018 EQT PROD CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2434313 Primary Facility 2015-12-16 Routine/Complete Inspection No Violations Noted Well tagged-shut in. Annulus open. Equipment-E&S controls-well site good.
2698844 Primary Facility 2018-02-27 Routine/Complete Inspection No Violations Noted This well is a part of a plugging consent order. The well is shut in and not equipped for production. The well head casing is sound and not leaking.
2784323 Primary Facility 2018-10-04 Plugging(Includes Plugged/Mined Through) No Violations Noted Records for this well show 2" production tubing to a depth of 3050'. The Rig crew could not get their tools deeper than 1486' where they sat down on something. At the time of this inspection they were getting ready to run back in the well bore with a smaller tool string to attempt to get to the attainable TD. All well paperwork and equipment on site looked ok.
2785035 Primary Facility 2018-10-05 Plugging(Includes Plugged/Mined Through) No Violations Noted Records for this well show 2" production tubing to a depth of 3050'. The Rig crew could not get their tools deeper than 1486' where they sat down on something. At the time of this inspection they were getting ready to run back in the well bore with a smaller tool string to attempt to get to the attainable TD. All well paperwork and equipment on site looked ok.

On this return date the rig crew ran a camera and determined that the 2" well tubing is parted below 200'. They plan on pulling the parted tubing out of the well bore and will attempt to get an overshot onto the tubing to attempt to continue plugging on this coming Monday. The crew was gone from site when I stopped by and all equipment on site looked ok.

For data sources see[6]

References