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37-005-25310

Well Details

Well ID: 37-005-25310
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Redbank Township
Operator Name: SNYDER BROS INC
Well Pad ID:
Farm/Lease Name: GLENN C. SHICK SR 4-101
License Status: ACTIVE
Spud Date:
Permit Date: 1994-02-22
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.009266
Longitude: -79.291388

For data sources see[1][2][3]

Well History

Date Event
1994-02-22 New Permit Application
1994-03-16 Performed Spud Operation
1994-03-22 Drilling Completion
1994-04-04 Perforation
1994-04-18 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1996 SNYDER BROS INC 8469 214 40.77 214 0.00 0
1997 SNYDER BROS INC 11747 328 146.71 328 0.00 0
1998 SNYDER BROS INC 8947 327 25.73 327 0.00 0
1999 SNYDER BROS INC 7654 342 28.78 342 0.00 0
2000 SNYDER BROS INC 7057 322 0.00 0 0.00 0
2001 SNYDER BROS INC 5971 341 127 341 0.00 0
2002 SNYDER BROS INC 4859 346 0.00 0 0.00 0
2003 SNYDER BROS INC 3765 263 58.16 263 0.00 0
2004 SNYDER BROS INC 5219 310 5.2 310 0.00 0
2005 SNYDER BROS INC 5574 357 153 357 0.00 0
2006 SNYDER BROS INC 4276.00 284 108.00 284 0.00 0
2007 SNYDER BROS INC 4487.00 365 0.00 0 0.00 0
2008 SNYDER BROS INC 3396.00 335 0.00 0 0.00 0
2009 SNYDER BROS INC 3106.00 325 0.00 0 0.00 0
2010 SNYDER BROS INC 2,881.00 319 0.00 0 0.00 0
2011 SNYDER BROS INC 3,679.00 302 0.00 0 0.00 0
2012 SNYDER BROS INC 2,880.00 321 0.00 0 0.00 0
2013 SNYDER BROS INC 2,637.00 353 0.00 0 0.00 0
2014 SNYDER BROS INC 2,595.00 343 60.00 343 0.00 0
2015 SNYDER BROS INC 2,995.00 365 0.00 0 0.00 0
2016 SNYDER BROS INC 2,408.00 345 0.00 0 0.00 0
2017 SNYDER BROS INC 2,438.00 313 0.00 0 0.00 0
2018 SNYDER BROS INC 2,124.00 322 7.60 27 0.00 0
2019 SNYDER BROS INC 2,484.00 326 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2002 SNYDER BROS INC Brine 25.00 Bbl Road Spreading
2003 SNYDER BROS INC Brine 45.00 Bbl Brine or Industrial Waste Treatment Plt
2004 SNYDER BROS INC Brine 35.00 Bbl Road Spreading
2005 SNYDER BROS INC Brine 55.00 Bbl Reuse other than road spreading 3701921388
2006 SNYDER BROS INC Brine 45.00 Bbl Reuse other than road spreading
2006 SNYDER BROS INC Brine 15.00 Bbl Road Spreading
2008 SNYDER BROS INC Brine 45.00 Bbl Reuse other than road spreading
2011 SNYDER BROS INC Produced Fluid 40.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2014 SNYDER BROS INC Produced Fluid 20.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2014 SNYDER BROS INC Produced Fluid 20 Bbl CENT WASTE TRT FAC NPDES PA0101508
2017 SNYDER BROS INC Produced Fluid 16.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1772757 Primary Facility 2009-02-27 Routine/Complete Inspection Violation(s) Noted nspection performed as a follow-up to an oil spill which occurred and was reported to the Department on 02/20/09. Vince Yantko, ER Team responded to the spill report and a copy of the incident report is attacehed. Noted that the underflow dams which had been constructed onsite were functioning properly, and that any oil was accumatling on top of the water behind the underflow dams. Saw no visible evidence on the surface of the ground of any oil discharge, nor was there any evidence of oil contamination entering Redbank Creek. There were two roll off dumpsters located onsite, both of which were lined and covered. The operator should continue to monitor the site and spill control measures should remain onsite until all of the evidence of oil contamination is abated.
1779672 Primary Facility 2009-03-31 Compliance Evaluation No Violations Noted nspection performed as a follow-up to an oil spill which occurred and was reported to the Department on 02/20/09. Saw no visible evidence on the surface of the ground of any oil discharge, nor was there any evidence of oil contamination entering Redbank Creek. In addition there was no observed evidence of oil contamination accumulated beind the underflow dams implemented during the spill cleanup.
215991 Primary Facility 1994-06-10 Routine/Complete Inspection No Violations Noted E&S OK; TWO TANKS
216108 Primary Facility 1994-08-12 Routine/Complete Inspection No Violations Noted E&S OK; TANK
216237 Primary Facility 1994-09-29 Site Restoration No Violations Noted SITE RESTORED; TANK
923765 Primary Facility 2000-03-14 Routine/Complete Inspection No Violations Noted Tag, 2 tanks, e&s ok.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1772757 557397 02/20/2009 2009-02-20 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
557397 243354 NOV - Notice of Violation Comply/Closed 2009-03-31
557397 251251 CACP - Consent Assessment of Civil Penalty Comply/Closed 2009-10-16 2009-10-16 $3,000.00 $3,000.00

For data sources see[7]

References