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37-005-25703

Well Details

Well ID: 37-005-25703
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Kittanning Township
Operator Name: SNYDER BROS INC
Well Pad ID:
Farm/Lease Name: EDWARD L. ECHNOZ 2-305
License Status: ACTIVE
Spud Date:
Permit Date: 1996-09-09
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.771783
Longitude: -79.478573

For data sources see[1][2][3]

Well History

Date Event
1996-09-09 New Permit Application
1996-10-22 Performed Spud Operation
1996-10-25 Drilling Completion
1996-11-11 Perforation
1997-04-07 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1997 SNYDER BROS INC 28752 258 0.00 0 0.00 0
1998 SNYDER BROS INC 32761 363 0.00 0 0.00 0
1999 SNYDER BROS INC 19373 372 0.00 0 0.00 0
2000 SNYDER BROS INC 14864 352 0.00 0 0.00 0
2001 SNYDER BROS INC 1287 370 0.00 0 0.00 0
2002 SNYDER BROS INC 9332 364 0.00 0 0.00 0
2003 SNYDER BROS INC 8006 356 0.00 0 0.00 0
2004 SNYDER BROS INC 8014 357 0.00 0 0.00 0
2005 SNYDER BROS INC 7541 356 0.00 0 0.00 0
2006 SNYDER BROS INC 5702.00 368 0.00 0 0.00 0
2007 SNYDER BROS INC 6197.00 365 0.00 0 0.00 0
2008 SNYDER BROS INC 5687.00 356 0.00 0 0.00 0
2009 SNYDER BROS INC 4953.00 354 0.00 0 0.00 0
2010 SNYDER BROS INC 2,687.00 235 0.00 0 0.00 0
2011 SNYDER BROS INC 4,535.00 333 0.00 0 0.00 0
2012 SNYDER BROS INC 4,103.00 363 0.00 0 0.00 0
2013 SNYDER BROS INC 3,745.00 361 0.00 0 0.00 0
2014 SNYDER BROS INC 3,661.00 365 0.00 0 0.00 0
2015 SNYDER BROS INC 3,324.00 365 0.00 0 0.00 0
2016 SNYDER BROS INC 3,424.00 362 0.00 0 0.00 0
2017 SNYDER BROS INC 3,217.00 361 0.00 0 0.00 0
2018 SNYDER BROS INC 2,275.00 363 0.00 0 0.00 0
2019 SNYDER BROS INC 3,205.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2015 SNYDER BROS INC Produced Fluid 25 Bbl CENT WASTE TRT FAC NPDES PA0095273
2015 SNYDER BROS INC Produced Fluid 25.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2407251 Primary Facility 2015-09-04 Routine/Complete Inspection No Violations Noted Access shared with ag field. At the time of inspection well appears equipped for production. Well tag present affixed in a permanent manner. Site permanently stabilized. No E&S issues in relation to site and/or access road. Brine tank appears to be compromised with very slow dripping observed at the base of the tank. Dripping localized to gravel containment area. Called Operator (John) from well site and recommended Operator follow-up with Department upon investigation of reported concerns. Violations may be forthcoming pending Departmental investigation.
2407252 Primary Facility 2015-09-08 Administrative/File Review No Violations Noted Operator (John) called Department on 9/8/2015 @ 10:30am in response to Department call on 9/4/2015 regarding structurally integrity of brine tank. Operator reported no measurable release occurred and the brine tank was removed from site and ground beneath removed brine tank stabilized.
2407255 Primary Facility 2015-09-09 Routine/Partial Inspection No Violations Noted Inspection performed as a follow-up to inspection if 9/4/2105 (ID# 2407251). Compromised brine tank has been removed from site. No leaks/spills (i.e. stained soil/gravel and/or dead or distressed vegetation) observed. Ground beneath removed brine tank stabilized. No E&S issues in relation to site. Department recommends Operator continue to perform routine monitoring and maintenance of site in order to prevent a potential pollution event from occurring.
2472922 Primary Facility 2016-04-08 Routine/Complete Inspection No Violations Noted Well tagged-in production. The 7"x4 1/2" well head casing and meter set look ok.

For data sources see[7]

References