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37-005-28693

Well Details

Well ID: 37-005-28693
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Mahoning Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: STATE GAME LANDS 137 35
License Status: ACTIVE
Spud Date:
Permit Date: 2006-04-27
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.993225
Longitude: -79.359795

For data sources see[1][2][3]

Well History

Date Event
2006-04-27 New Permit Application
2006-08-10 Performed Spud Operation
2006-08-18 Drilling Completion
2006-08-23 Perforation
2008-01-15 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 EXCO RESOURCES PA INC 0.00 0 0.00 0 0.00 0
2006 EXCO RESOURCES PA INC 0.00 0 0.00 0 0.00 0
2007 EXCO RESOURCES PA INC 0.00 0 0.00 0 0.00 0
2008 EXCO RESOURCES PA INC 1558.37 366 0.00 0 0.00 0
2009 EXCO RESOURCES PA INC 1828.00 365 0.00 0 0.00 0
2010 EXCO RESOURCES PA INC 1,599.00 365 0.00 0 0.00 0
2011 EXCO RESOURCES PA INC 1,483.00 365 0.00 0 0.00 0
2012 EXCO RESOURCES PA LLC 1,293.00 366 0.00 0 0.00 0
2013 EXCO RESOURCES PA LLC 1,328.00 365 0.00 0 0.00 0
2014 EXCO RESOURCES PA LLC 1,154.64 334 15.14 365 0.00 0
2015 EXCO RESOURCES PA LLC 970.46 362 0.00 0 0.00 0
2016 ALLIANCE PETRO CO LLC 425.00 183 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 933.00 365 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 903.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 647.00 334 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1535856 Primary Facility 2006-04-12 Site Restoration No Violations Noted WELL STAKED/SITE NOT MADE/WAIVER OK
1558979 Primary Facility 2006-08-16 Drilling/Alteration No Violations Noted WELL SPUD 08/11/06/PIT OK/
2269661 Primary Facility 2014-05-06 Administrative/File Review In Compliance with Policy SPILL. Admin inspt in response to reported release by Doug Byers to SWRO on 5/5/2014 at 1545.
2269704 Primary Facility 2014-05-06 Incident- Response to Accident or Event Violation(s) Noted On-site inspt in response to admin inspt (record 2269661) for the 5/5/14 reported spill of 22 bbl brine into earthen dike.Dept met EHS Coordinator Dan Chimino on-site.At time of inspt, no visible fluids remain.Impacted materials not yet excavated.Ground staining observed in left half of dike when facing valve.Staining leads to drain that empties dike.Per Mr. Chimino, after delineation, appears brine drained out of valve & extended several ft into down-gradient grassy area.Tank was immediately emptied & valve is to be replaced.Removal of tanks & excavation of contaminated materials scheduled for next week.Mr. Chimino also stated 4 absorbent pads were utilized to soak up localized oil sheen near valve.Dept recom'ds Opr sample for all fluids released for site remediation.WT present.Drilling occurred 8/11/2006-8/18/2006.AR stable.E-mail documenting events surrounding spill requested.Dept requests disposal records & manifests upon final disposition of wastes.Viols issued under 25 PA CODE 78.57A for this reportable release of production fluids.
2305785 Primary Facility 2014-09-18 Follow-up Inspection Outstanding Violations - No Viols Req'd A discharge of production fluids ocurred in May 2014 at the site. Operator had initiated remediation activities and excavated the affected media and submitted a site chracaterization report for the site. Site had not as of yet been regraded seeded or mulched. There was no observed accelerated erosion or sedimentation in relation to the site or access road. Brine tank located onsite and it appeared to be in sound condition.
2352593 Primary Facility 2015-03-12 Compliance Evaluation No Violations Noted Well appeared ot be equipped for production. Brine tank located onsite and it appeared to be in sound condition. There was no observed accelerated erosion or sedimenation in relation to the site or access road. Area that had been affected by the discharge had been effectively remediated.
2507348 Primary Facility 2016-07-28 Routine/Complete Inspection No Violations Noted Well tagged-in production. Annulus open. Well head casing-equipment-1000 gallon plastic tank-dike ok.
2731423 Primary Facility 2018-05-18 Routine/Complete Inspection No Violations Noted This well is tagged and in production. The annulus is open. The well head casing, piping, equipment and small plastic fluid collection tank look ok.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2269704 695480 05/06/2014 2014-05-06 78.57 - Failure to post pit approval number Administrative Violation issued for reportable release of production fluids from brine tank.

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
695480 310917 NOV - Notice of Violation Superseded 2017-12-08
695480 360241 CACP - Consent Assessment of Civil Penalty Comply/Closed 2017-12-08 2017-12-08 $27,000.00 $27,000.00

For data sources see[6]

References