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Well ID: 37-005-29781 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Plumcreek Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: HELVETIA COAL MINING CO 9 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2008-03-31 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.727877 | |
Longitude: -79.358327 |
Date | Event |
---|---|
2008-03-31 | New Permit Application |
2008-07-23 | Performed Spud Operation |
2008-08-04 | Drilling Completion |
2008-08-11 | Perforation |
2009-03-12 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | PHILLIPS EXPLORATION INC | 1959.00 | 92 | 0.00 | 0 | 0.00 | 0 |
2009 | PHILLIPS EXPLORATION INC | 6035.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | PHILLIPS EXPLORATION INC | 7,632.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | PHILLIPS EXPLORATION INC | 7,207.00 | 352 | 0.00 | 0 | 0.00 | 0 |
2012 | XTO ENERGY INC | 6,102.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | XTO ENERGY INC | 4,650.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | XTO ENERGY INC | 4,104.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | XTO ENERGY INC | 3,629.83 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | XTO ENERGY INC | 2,852.00 | 338 | 0.00 | 0 | 0.00 | 0 |
2017 | ALLIANCE PETRO CO LLC | 1,904.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2018 | ALLIANCE PETRO CO LLC | 2,943.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 2,485.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2014 | XTO ENERGY INC | Produced Fluid | 43.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2014 | XTO ENERGY INC | Produced Fluid | 43 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2015 | XTO ENERGY INC | Produced Fluid | 23 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2015 | XTO ENERGY INC | Produced Fluid | 23.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1726078 | Primary Facility | 2008-07-28 | Drilling/Alteration | No Violations Noted | Rig drilling. Pit/E&S controls OK. |
1820747 | Primary Facility | 2009-08-14 | Site Restoration | No Violations Noted | Drilling was completed on 08/04/08. Well appeared to be equipped for & in production. Brine tank located onsite and appeared to be in sound condition. Vegetatiove cocver appeared to meet the 70% uniform cov erage criteria. No accelerated erosion & sedimentation observed in relation to the well-site or access road. |
2252829 | Primary Facility | 2014-03-12 | Routine/Complete Inspection | No Violations Noted | Well appeared to be equipped for production at the time of the inspection. Brine tank located onsite and it appeared to be in sound condition. There was no observed accelerated erosion or sedimentation observed in relation to the site or access road. |
2527495 | Primary Facility | 2016-10-13 | Routine/Complete Inspection | No Violations Noted | Well tagged-in production. Annulus was shut. Well head casing-equipment-grounded 100 bbl plastic tank looked ok. |
For data sources see[7]