X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-005-30319

Well Details

Well ID: 37-005-30319
Loading map...
Country: United States
State: Pennsylvania
County: Armstrong
Municipality: North Buffalo Township
Operator Name: MDS ENERGY DEV LLC
Well Pad ID:
Farm/Lease Name: KATHY A DREYER 1-17
License Status:
Spud Date:
Permit Date: 2009-04-14
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.786841
Longitude: -79.593809

For data sources see[1][2][3]

Well History

Date Event
2009-04-14 New Permit Application
2009-06-10 Performed Spud Operation
2009-06-15 Drilling Completion
2010-06-17 Perforation
2013-07-29 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 MDS ENERGY LTD 6,091.00 261 0.00 0 0.00 0
2011 MDS ENERGY LTD 13,925.00 362 0.00 0 0.00 0
2012 MDS ENERGY LTD 11,378.00 360 0.00 0 0.00 0
2013 MDS ENERGY LTD 7,551.00 354 0.00 0 0.00 0
2014 MDS ENERGY LTD 5,927.00 352 0.00 0 0.00 0
2015 MDS ENERGY DEV LLC 3,402.00 309 0.00 0 0.00 0
2016 MDS ENERGY DEV LLC 4,897.00 323 0.00 0 0.00 0
2017 MDS ENERGY DEV LLC 5,449.00 338 0.00 0 0.00 0
2018 MDS ENERGY DEV LLC 2,713.00 282 0.00 0 0.00 0
2019 MDS ENERGY DEV LLC 3,375.00 286 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 MDS ENERGY LTD Produced Fluid 60.00 Bbl REUSE OTHER THAN ROAD SPREADING
2014 MDS ENERGY LTD Produced Fluid 52.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2014 MDS ENERGY LTD Produced Fluid 52 Bbl CENT WASTE TRT FAC NPDES PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1808569 Primary Facility 2009-06-18 Routine/Complete Inspection No Violations Noted Drilling was to have commenced on 06/10/09. Drilling appeared to have been completed at the time of the inspection. Below grade pit onsite had more than the two feet of required freeboard. Observed no accelerated erosion & sedimentation in relation to the well-site or access road. The operartor should continue to monitor the site for accelerated erosion & sedimentation until well development and final restoration activities are completed.
2226693 Primary Facility 2013-12-05 Routine/Complete Inspection No Violations Noted Well was equipped for production and a brine tank was located onsite. Brine tank appeared to be in sound condition. There was no accelerated erosion or sedimentation observed in relation to the site or access road.

For data sources see[7]

References