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37-019-00712

Well Details

Well ID: 37-019-00712
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Country: United States
State: Pennsylvania
County: Butler
Municipality: Clearfield Township
Operator Name: REDMILL DRILLING
Well Pad ID:
Farm/Lease Name: CF KEASEY 10611
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.829390
Longitude: -79.733510

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1987-03-25 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1990 DAMSON OIL CORP 653.00 365 0.00 0 0.00 0
1991 PARKER & PARSLEY DEV LP 427.00 364 0.00 0 0.00 0
1992 PARKER & PARSLEY DEV LP 495.00 368 0.00 0 0.00 0
1993 PARKER & PARSLEY DEV LP 651.00 364 0.00 0 0.00 0
1994 PARKER & PARSLEY DEV LP 843.00 366 0.00 0 0.00 0
1995 RANGE OPR CO 315.00 153 0.00 0 0.00 0
1996 RANGE OPR CO 540 365 0.00 0 0.00 0
1999 BLX INC 975 370 0.00 0 0.00 0
2000 BLX INC 871 364 0.00 0 0.00 0
2001 BLX INC 829 333 0.00 0 0.00 0
2002 BLX INC 865.42 330 0.00 0 0.00 0
2003 BLX INC 859.65 337 0.00 0 0.00 0
2004 BLX INC 1016.86 365 0.00 0 0.00 0
2005 BLX INC 938.14 364 0.00 0 0.00 0
2006 BLX INC 1069.00 364 0.00 0 0.00 0
2007 BLX INC 818.00 365 0.00 0 0.00 0
2008 BLX INC 817.00 365 0.00 0 0.00 0
2009 BLX INC 811.00 360 0.00 0 0.00 0
2010 BLX INC 988.69 365 0.00 0 0.00 0
2011 BLX INC 688.22 339 0.00 0 0.00 0
2012 BLX INC 1,005.24 365 0.00 0 0.00 0
2013 REDMILL DRILLING 840.53 365 0.00 0 0.00 0
2014 REDMILL DRILLING 709.89 364 0.00 0 0.00 0
2015 REDMILL DRILLING 812.12 364 0.00 0 0.00 0
2016 REDMILL DRILLING 864.91 364 0.00 0 0.00 0
2017 REDMILL DRILLING 707.17 365 0.00 0 0.00 0
2018 REDMILL DRILLING 687.29 365 0.00 0 0.00 0
2019 SME WELL SVC INC 142.15 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2655253 Primary Facility 2017-10-31 Routine/Partial Inspection No Violations Noted At the time of inspection, well appeared it is producible. The valve was one that is difficult to say if it is open or not. Production was reported for last year, and produced nearly the entire year. Well integrity appeared to be in good condition, with no signs of any leaks or spills at the site. Some rust on top of wellhead, but corrosion was superficial. Annulus for casing was closed. Well is hooked up to a long drip and there is a tie-in about 20 yards away. Well was properly labeled.

For data sources see[6]

References