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37-019-00741

Well Details

Well ID: 37-019-00741
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Country: United States
State: Pennsylvania
County: Butler
Municipality: Winfield Township
Operator Name: REDMILL DRILLING
Well Pad ID:
Farm/Lease Name: SARAH S DODDS 14251
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.761770
Longitude: -79.767640

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1987-01-01 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1990 DAMSON OIL CORP 1100.00 365 0.00 0 0.00 0
1991 PARKER & PARSLEY DEV LP 1076.00 365 0.00 0 0.00 0
1992 PARKER & PARSLEY DEV LP 114.00 366 0.00 0 0.00 0
1993 PARKER & PARSLEY DEV LP 1342.00 365 0.00 0 0.00 0
1994 PARKER & PARSLEY DEV LP 1276.00 365 0.00 0 0.00 0
1995 RANGE OPR CO 594.00 153 0.00 0 0.00 0
1996 RANGE OPR CO 1160 365 0.00 0 0.00 0
1999 BLX INC 667 373 0.00 0 0.00 0
2000 BLX INC 947 362 0.00 0 0.00 0
2001 BLX INC 912 334 0.00 0 0.00 0
2002 BLX INC 952 294 0.00 0 0.00 0
2003 BLX INC 801 331 0.00 0 0.00 0
2004 BLX INC 1041 365 0.00 0 0.00 0
2005 BLX INC 1026 362 0.00 0 0.00 0
2006 BLX INC 955.00 364 0.00 0 0.00 0
2007 BLX INC 854.00 365 0.00 0 0.00 0
2008 BLX INC 853.00 364 0.00 0 0.00 0
2009 BLX INC 1089.00 359 0.00 0 0.00 0
2010 BLX INC 1,031.00 363 0.00 0 0.00 0
2011 BLX INC 753.00 364 0.00 0 0.00 0
2012 BLX INC 1,157.00 344 0.00 0 0.00 0
2013 REDMILL DRILLING 1,052.00 365 0.00 0 0.00 0
2014 REDMILL DRILLING 1,013.00 364 0.00 0 0.00 0
2015 REDMILL DRILLING 983.00 365 0.00 0 0.00 0
2016 REDMILL DRILLING 889.00 364 0.00 0 0.00 0
2017 REDMILL DRILLING 429.00 335 0.00 0 0.00 0
2018 REDMILL DRILLING 375.00 363 0.00 0 0.00 0
2019 SME WELL SVC INC 277.00 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2695516 Primary Facility 2018-02-12 Routine/Partial Inspection No Violations Noted At the time of inspection, well appeared to be producing. Well integrity appeared to be in good condition with no signs of any leaks or spills. There was some minor rust on the well, but does not appear to be posing any issues. The well was properly labeled. Appears to be 5 1/2" casing inside of 7". Well is hooked up to a vertical drip. There was also a meter and line heater. Production for 2017 was reported as 429 mcf for 335 days.

For data sources see[6]

References