X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-027-20563

Well Details

Well ID: 37-027-20563
Loading map...
Country: United States
State: Pennsylvania
County: Centre
Municipality: Burnside Township
Operator Name: CAPITAL OIL & GAS INC
Well Pad ID:
Farm/Lease Name: C.O.P. TRACT 257 41
License Status: ACTIVE
Spud Date:
Permit Date: 1991-09-03
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.111286
Longitude: -77.917595

For data sources see[1][2][3]

Well History

Date Event
1991-09-03 New Permit Application
1991-09-20 Performed Spud Operation
1991-09-25 Drilling Completion
1991-09-30 Perforation
1992-01-01 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 EQUITABLE PROD EASTERN STATES EXPLORATION INC 6493.00 30 0.00 0 0.00 0
1992 EQUITABLE PROD EASTERN STATES EXPLORATION INC 62476.00 360 0.00 0 0.00 0
1994 EQUITABLE PROD EASTERN STATES EXPLORATION INC 30457.00 365 0.00 0 0.00 0
1995 EQUITABLE PROD EASTERN STATES EXPLORATION INC 27545.00 365 0.00 0 0.00 0
1996 EQUITABLE PROD EASTERN STATES EXPLORATION INC 24772 365 0.00 0 0.00 0
1997 EQUITABLE PROD EASTERN STATES EXPLORATION INC 22712 365 0.00 0 0.00 0
1998 EQUITABLE PROD EASTERN STATES EXPLORATION INC 21900 365 0.00 0 0.00 0
1999 EQUITABLE PROD EASTERN STATES EXPLORATION INC 17054 365 0.00 0 0.00 0
2000 EQUITRANS INC 15352 365 0.00 0 0.00 0
2001 EQUITABLE PROD EASTERN STATES EXPLORATION INC 14405 365 0.00 0 0.00 0
2003 EQT PROD CO 13570 365 0.00 0 0.00 0
2004 EQT PROD CO 13615 366 0.00 0 0.00 0
2005 EQT PROD CO 5153 151 0 151 0.00 0
2006 EQT PROD CO 0.00 0 0.00 0 0.00 0
2007 EQT PROD CO 0.00 0 0.00 0 0.00 0
2008 EQT PROD CO 0.00 0 0.00 0 0.00 0
2009 EQT PROD CO 0.00 0 0.00 0 0.00 0
2010 EQT PROD CO 0.00 0 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0
2012 EQT PROD CO 0.00 0 0.00 0 0.00 0
2013 EQT PROD CO 0.00 0 0.00 0 0.00 0
2014 EQT PROD CO 0.00 0 0.00 0 0.00 0
2015 NCL NATURAL RESOURCES LLC 0.00 0 0.00 0 0.00 0
2016 NCL NATURAL RESOURCES LLC 7,020.00 365 0.00 0 0.00 0
2017 CAPITAL OIL & GAS INC 3,243.00 333 0.00 0 0.00 0
2018 CAPITAL OIL & GAS INC 2,187.00 325 0.00 0 0.00 0
2019 CAPITAL OIL & GAS INC 350.00 339 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1996 EQUITABLE PROD EASTERN STATES EXPLORATION INC Brine 32.00 Bbl Road Spreading
1997 EQUITABLE PROD EASTERN STATES EXPLORATION INC Brine 15.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
1998 EQUITABLE PROD EASTERN STATES EXPLORATION INC Brine 19.00 Bbl Brine or Industrial Waste Treatment Plt PA0020486
1999 EQUITABLE PROD EASTERN STATES EXPLORATION INC Brine 28.00 Bbl Brine or Industrial Waste Treatment Plt PA0020486
2001 EQUITABLE PROD EASTERN STATES EXPLORATION INC Brine 23.00 Bbl Road Spreading SEVERAL TWPS.
2005 NCL NATURAL RESOURCES LLC Brine 35.00 Bbl Brine or Industrial Waste Treatment Plt PA0101508
2005 NCL NATURAL RESOURCES LLC Brine 35.00 Bbl Road Spreading
2006 NCL NATURAL RESOURCES LLC Brine 40.00 Bbl Brine or Industrial Waste Treatment Plt PA0101508
2010 NCL NATURAL RESOURCES LLC Produced Fluid 33 Bbl CENT WASTE TRT FAC NPDES PA0101508
2010 NCL NATURAL RESOURCES LLC Produced Fluid 33.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2011 NCL NATURAL RESOURCES LLC Produced Fluid 25 Bbl CENT WASTE TRT FAC NPDES PA0101508
2011 NCL NATURAL RESOURCES LLC Produced Fluid 25.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2018 CAPITAL OIL & GAS INC Produced Fluid 60.00 Bbl INJECTION DISPOSAL WELL 34-151-22089

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
214705 Primary Facility 1992-07-14 Site Restoration No Violations Noted SITE RESTORED; TANK
215102 Primary Facility 1992-12-15 Routine/Complete Inspection No Violations Noted E&S OK; TANK
2450807 Primary Facility 2016-01-29 Administrative/File Review Violation(s) Noted Inspection record sent 1/12/16. Violation logged 1/29/16 due to well not being registered to NCL yet.
2680856 Primary Facility 2017-12-07 Routine/Complete Inspection No Violations Noted 4-1/2" collar on the wellhead is leaking gas.

The weather is 35 Deg. F, cloudy and windy at time of inspection. Routine inspection of Capital Oil and Gas Inc., C.O.P. TRACT 257 41 Pad on December 7, 2017. This well was shut in upon arrival to location, and has been opened and set to producing by the operator during inspection. Annulus is open and vented at time of inspection. 100% LEL and 7% combustible gas was detected at the 4-1/2" collar of the wellhead. No violations noted, but discussed follow up inspection after equipment with gas leak is repaired. Capital Oil and Gas Inc. representatives during inspection: Beau Martin ¿ Production Superintendent. DEP Representative ¿ Ulyana Trynovich, Oil and Gas Inspector.

2680863 Primary Facility 2018-01-10 Follow-up Inspection No Violations Noted The weather is 36 Deg. F, sunny and windy at time of inspection. Follow up inspection of Capital Oil and Gas Inc., C.O.P. TRACT 257 41 Pad on January 10, 2018.

Equipment with the gas leak found previously, has been repaired. Annulus is open and vented at time of inspection. 0% combustible gas was detected at the annulus vent or in the area immediately surrounding the well. No violations noted. Capital Oil and Gas Inc. representatives during inspection: Beau Martin ¿ Production Superintendent. DEP Representative ¿ Ulyana Trynovich, Oil and Gas Inspector.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2450807 746343 2016-01-29 2017-02-17 OGA3223 Administrative
2450807 746344 2016-01-29 2017-02-17 OGA 3222(A) Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
746343 334710 NOV - Notice of Violation 2017-02-17
746343 351129 CACP - Consent Assessment of Civil Penalty COMP - Completed 2017-02-17 2017-02-17 $8,150.00 $8,150.00
746344 334710 NOV - Notice of Violation 2017-02-17
746344 351129 CACP - Consent Assessment of Civil Penalty COMP - Completed 2017-02-17 2017-02-17 $8,150.00 $8,150.00

For data sources see[7]

References