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Well ID: 37-031-22700 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Clarion | |
Municipality: Hawthorn Borough | |
Operator Name: R B ROBERTSON & SON GAS & OIL CO LP | |
Well Pad ID: | |
Farm/Lease Name: H JEROME HEFFNER 3 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 1994-03-28 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.020350 | |
Longitude: -79.288930 |
Date | Event |
---|---|
1994-03-28 | New Permit Application |
1994-11-16 | Performed Spud Operation |
1994-11-22 | Drilling Completion |
1995-02-13 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2001 | RB ROBERTSON & SON GAS & OIL | 12874 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | RB ROBERTSON & SON GAS & OIL | 6079 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | RB ROBERTSON & SON GAS & OIL | 9050 | 299 | 0.00 | 0 | 0.00 | 0 |
2004 | RB ROBERTSON & SON GAS & OIL | 8175 | 325 | 0.00 | 0 | 0.00 | 0 |
2005 | RB ROBERTSON & SON GAS & OIL | 6152 | 325 | 0.00 | 0 | 0.00 | 0 |
2006 | RB ROBERTSON & SON GAS & OIL | 5930.00 | 355 | 0.00 | 0 | 0.00 | 0 |
2007 | RB ROBERTSON & SON GAS & OIL | 6460.00 | 350 | 0.00 | 0 | 0.00 | 0 |
2008 | RB ROBERTSON & SON GAS & OIL | 6407.00 | 347 | 0.00 | 0 | 0.00 | 0 |
2009 | RB ROBERTSON & SON GAS & OIL | 3002.00 | 245 | 0.00 | 0 | 0.00 | 0 |
2010 | RB ROBERTSON & SON GAS & OIL | 4,499.00 | 273 | 0.00 | 0 | 0.00 | 0 |
2011 | RB ROBERTSON & SON GAS & OIL | 4,141.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | RB ROBERTSON & SON GAS & OIL | 3,267.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | RB ROBERTSON & SON GAS & OIL | 2,439.67 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | R B ROBERTSON & SON GAS & OIL CO LP | 1,250.33 | 273 | 0.00 | 0 | 0.00 | 0 |
2015 | R B ROBERTSON & SON GAS & OIL CO LP | 1,103.67 | 303 | 0.00 | 0 | 0.00 | 0 |
2016 | R B ROBERTSON & SON GAS & OIL CO LP | 1,332.33 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | R B ROBERTSON & SON GAS & OIL CO LP | 2,060.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | R B ROBERTSON & SON GAS & OIL CO LP | 2,960.50 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | R B ROBERTSON & SON GAS & OIL CO LP | 1,809.50 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
216392 | Primary Facility | 1994-12-01 | Routine/Complete Inspection | No Violations Noted | |
2788313 | Primary Facility | 2018-10-11 | Routine/Partial Inspection | No Violations Noted | At the time of inspection, well was producing. Gas flow could be heard. Well integrity appeared to be in good condition, with no signs of any leaks. There was only some minor rust on the well. The well was hooked up to a separator which had a gauge reading 48 psi. The chart in the meter house hadn't been changed since 6/2. The well was also equipped with a rabbit. A 75 bbl poly tank was also being used. I did not see a label on the well. Production was reported in 2017 as 2060 mcf for 365 days. |
For data sources see[6]