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37-059-23205

Well Details

Well ID: 37-059-23205
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Country: United States
State: Pennsylvania
County: Greene
Municipality: Gilmore Township
Operator Name: CNX GAS CO LLC
Well Pad ID:
Farm/Lease Name: TRIUMPH WELL BH-3A
License Status: ACTIVE
Spud Date:
Permit Date: 2002-10-02
Well Type: COALBED METHANE
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 39.774846
Longitude: -80.342468

For data sources see[1][2][3]

Well History

Date Event
2002-10-02 New Permit Application
2002-10-21 Performed Spud Operation
2003-01-26 Drilling Completion
2003-06-06 DEVIATED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2002 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2003 CNX GAS CO LLC 37847 137 0.00 0 0.00 0
2004 CNX GAS CO LLC 132890 365 0 365 0.00 0
2005 CNX GAS CO LLC 128423 365 0.00 0 0.00 0
2006 CNX GAS CO LLC 109948.00 365 0.00 0 0.00 0
2007 CNX GAS CO LLC 93005.00 365 0.00 0 0.00 0
2008 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2009 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1182579 Primary Facility 2002-10-24 Drilling/Alteration No Violations Noted tripping
1210775 Primary Facility 2003-01-31 Drilling/Alteration No Violations Noted drilling ahead
1282545 Primary Facility 2003-10-28 Routine/Complete Inspection No Violations Noted Pumpjack operating, compressor unit here, tanked fluids w/dike, bench ditched. Coalbed methane extraction wells bench restored w/wells operating. Routinely serviced.
1404477 Primary Facility 2004-12-20 Routine/Complete Inspection No Violations Noted Service rig on-site to replace down hole pump, in-line and producing, e/s ok

For data sources see[6]

References