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37-059-25267

Well Details

Well ID: 37-059-25267
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Country: United States
State: Pennsylvania
County: Greene
Municipality: Morris Township
Operator Name: CNX GAS CO LLC
Well Pad ID: 147993
Farm/Lease Name: CONRHEIN
License Status: Plugged and Abandoned
Spud Date:
Permit Date: 2009-08-13
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 40.004867
Longitude: -80.287747

For data sources see[1][2][3]

Well History

Date Event
2009-08-13 New Permit Application
2010-02-18 Performed Spud Operation
2014-11-10 Begin Plugging
2015-05-21 Finished Plugging

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2010 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2011 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2013 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2014 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2015 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2016 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 CNX GAS CO LLC Produced Fluid 39.59 Bbl INJECTION DISPOSAL WELL 34-105-23619
2013 CNX GAS CO LLC Produced Fluid 494.44 Bbl REUSE OTHER THAN ROAD SPREADING
2013 CNX GAS CO LLC Produced Fluid 10.11 Bbl INJECTION DISPOSAL WELL 34-031-27177
2013 CNX GAS CO LLC Produced Fluid 14.22 Bbl INJECTION DISPOSAL WELL 34-013-20609
2013 CNX GAS CO LLC Produced Fluid 5.54 Bbl INJECTION DISPOSAL WELL 34-059-24202
2013 CNX GAS CO LLC Produced Fluid 0.53 Bbl INJECTION DISPOSAL WELL 34-119-28776
2015 CNX GAS CO LLC Drilling Fluid Waste 1,269.33 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CNX GAS CO LLC Produced Fluid 82.50 Bbl REUSE OTHER THAN ROAD SPREADING

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1867568 Primary Facility 2010-02-24 Routine/Complete Inspection No Violations Noted
1880487 Primary Facility 2010-03-24 Routine/Complete Inspection No Violations Noted Minor Modification to the ESCGP-1
1881423 Primary Facility 2010-04-27 Drilling/Alteration No Violations Noted WHIPSTOCK 23 MOVING, BUTCH'S ANCHOR SERVICE SETTING CONDUCTORS. PITS GOOD
1889660 Primary Facility 2010-05-18 Routine/Complete Inspection No Violations Noted The Department was at the above reference site to conduct a Waiver Inspection. The Operator has already built the site and is currently drilling Multiple Marcellus Wells on this pad. The Department approves the waiver for the 100 ft distance restriction to Bates Fork. Bates Fork is a tributary to Brown's Creek which is a High Quality Stream. The Department has reviewed the E/S plan and inspected the E/S Controls. All BMP's appear to be in good working order and the Operator should continue to inspect the site as needed..
1895051 Primary Facility 2010-06-24 Drilling/Alteration No Violations Noted HORIZONTAL MARCELLUS
1898832 Primary Facility 2010-06-21 Routine/Complete Inspection No Violations Noted Site and E/S Control in good condition.
2362794 Primary Facility 2015-03-24 Plugging(Includes Plugged/Mined Through) No Violations Noted Conserv rig on location in December, 2014 to plug CNX Marcellus lateral. Perf gun and wireline lost down hole.; left gun downhole; retrieved a lot of wirline. Set cast iron bridge plug @ 8000' and cemented from 8000' to 7525'; gel plug to 6500'; 2nd cement plug from 6500' to 6300'; get plug to 5300'; third cement plug from 5300 to 4750' over area where hole in 51/2' casing was found @ 5198'; TOC in 5 1/2" is 4370'; Bond log in 5 1/2' indicated no cement from 2750 to surface; Going to make cut @ 2740 to pull 5 1/2" casing out; Then a bond log will be run on 9 5/8" to confirm good cement bond or TOC as cement flash set and only 3 bbls was run down annulus.
2362871 Primary Facility 2015-04-10 Plugging(Includes Plugged/Mined Through) No Violations Noted Ran bond log behind the 9 5/8 from app 476 to surface; TOC is shown app.93' indicating a basket was placed on the casing; no cement bond from 93 feet down.;; will review with operator;
2787646 Primary Facility 2018-10-10 Routine/Complete Inspection No Violations Noted On Wednesday October 10, 2018 I conducted a routine-complete inspection at the NV17 Well Site located in Morris Township, Greene County.

Gas well NV17CCV (059-25267) was plugged in 2015 and a monument identifies the location and permit number.

No violations were identified during the inspection.

For data sources see[7]

References