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37-063-25563

Well Details

Well ID: 37-063-25563
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Green Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: CLYDE GREEN 3C636
License Status: ABANDONED
Spud Date: 1981-04-20
Permit Date: 1981-04-21
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.716663
Longitude: -78.984758

For data sources see[1][2][3]

Well History

Date Event
1981-04-20 Performed Spud Operation
1981-04-21 New Permit Application
1981-04-25 Drilling Completion
1981-05-06 Perforation
1981-10-05 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1994 195.00 365 0.00 0 0.00 0
1996 PENTEX ENERGY INC 90 365 0.00 0 0.00 0
1997 PENTEX ENERGY INC 0.00 0 0.00 0 0.00 0
1998 PENTEX ENERGY INC 38 28 0.00 0 0.00 0
1999 PENTEX ENERGY INC 144 216 0.00 0 0.00 0
2000 PENTEX ENERGY INC 0.00 0 0.00 0 0.00 0
2001 PENTEX ENERGY INC 0.00 0 0.00 0 0.00 0
2002 PENTEX ENERGY INC 0.00 0 0.00 0 0.00 0
2003 PENTEX ENERGY INC 0.00 0 0.00 0 0.00 0
2004 LINN OPR LLC 0.00 0 0.00 0 0.00 0
2006 LINN OPR INC 400.00 365 0.00 0 0.00 0
2007 LINN OPR INC 345.00 365 0.00 0 0.00 0
2008 XTO ENERGY INC 195.00 365 0.00 0 0.00 0
2009 XTO ENERGY INC 172.00 365 0.00 0 0.00 0
2010 XTO ENERGY INC 81.00 365 0.00 0 0.00 0
2011 XTO ENERGY INC 97.00 365 0.00 0 0.00 0
2012 XTO ENERGY INC 54.00 263 0.00 0 0.00 0
2013 XTO ENERGY INC 58.00 170 0.00 0 0.00 0
2014 XTO ENERGY INC 47.00 172 0.00 0 0.00 0
2015 XTO ENERGY INC 141.05 196 0.00 0 0.00 0
2016 XTO ENERGY INC 210.48 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 63.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 21.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 9.00 181 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2006 LINN OPR INC Brine 216.00 Bbl Brine or Industrial Waste Treatment Plt PA0095273
2009 XTO ENERGY INC Brine 57.00 Bbl Brine or Industrial Waste Treatment Plt PA0095273
2014 XTO ENERGY INC Produced Fluid 50.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2014 XTO ENERGY INC Produced Fluid 50 Bbl CENT WASTE TRT FAC NPDES PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2306864 Primary Facility 2014-09-24 Administrative/File Review In Compliance with Policy SPILL.
2306886 Primary Facility 2014-09-24 Incident- Response to Accident or Event Violation(s) Noted On-site inspt in response to admin inspt 2306864 for the reportable release of 9 bbl brine water onto ground.At time of inspt, excavation not yet commenced.Brine release reported to be the result of a porcupine chewing through tank.Stressed vegetation, visibly released minimal fluids remain localized to well site.Brine appears to have traveled slightly down-gradient to level ground before "settling".Opr in process of arranging delivery of roll-off box(es) to site.Excavation of contaminated soils to commence tomorrow morning (9/25) upon arrival of roll-off box(es).Damaged BT remains on-site.WT present, legible.Drilling occurred 4/20/81-4/25/81.
2311569 Primary Facility 2014-10-09 Follow-up Inspection Outstanding Violations - No Viols Req'd FUI in response to viols issued under record 2306886 (enf ID 315415).At time of inspection, all visibly impacted soils appear excavated. Site not yet temporarily stabilized. Per current regulations, upon temporary cessation of an earth disturbance activity or any stage or phase of an activity where a cessation of earth disturbance activities will exceed 4 days, the site shall be immediately seeded, mulched, or otherwise protected from accelerated erosion and sedimentation. Department recommends Operator temporarily stabilize site in order to prevent any additional pollution events from occurring.Outstanding violations exist, no new violations noted at this time.In accordance with the spill policy, 15 day initial report received 10/03/2014. The Operator will be utilizing Act 2 for site remediation.Requested formal written response to violations received on 10/03/2014.
2335768 Primary Facility 2015-01-12 Follow-up Inspection Outstanding Violations - No Viols Req'd FUI in response to violations issued under inspection record 2306886 (enf ID 315415) for the 9/24/14 reportable release of 9 bbl brine water onto ground.
2402334 Primary Facility 2015-08-25 Compliance Evaluation No Violations Noted On-site CEI in response to viols issued under record 2306886 (enf ID 315415) for 9/24/14 reportable release of 9 bbl brine water onto ground.At time of inspt, area of excavation not yet backfilled.Damaged BT previously removed from site.WT present, legible.Dept recommends Opr cont’ to monitor/maintain site to ensure >70% uniform and adequate veg is attained for final permanent stabilization of the site upon completion of backfilling of the site.In accordance with spill policy, 15 day initial report received 10/03/14 notifying the Dept that Opr will be utilizing Act 2 for site remediation.Act 2 approval received on 8/13/15.
2430061 Primary Facility 2015-12-03 Administrative/File Review In Compliance with Policy Admin inspection conducted in response to violations issued under inspection record 2306886 (enf ID 315415) for the reportable release of 9 bbl brine water.
2509149 Primary Facility 2016-08-08 Routine/Complete Inspection No Violations Noted system running no issues
2580843 Primary Facility 2017-04-10 Routine/Complete Inspection No Violations Noted Inspection conducted to assess site remediation as a reportable release of brine previously occurred at this site.

At time of inspection, well appears equipped for production. Well tag present, legible. No brine tank on-site.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2306886 705590 09/24/2014 2014-09-24 78.57(A)* - Discharge of brine and other fluids on or into the ground or into the waters of the Commonwealth without a permit. Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
705590 315415 NOV - Notice of Violation Superseded 2018-04-30
705590 363720 CPA - Civil Penalty Assessment Comply/Closed 2018-06-06 2018-06-06 $70,000.00 $70,000.00

For data sources see[7]

References