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37-063-34158

Well Details

Well ID: 37-063-34158
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Conemaugh Township
Operator Name: US ENERGY EXPLORATION CORP
Well Pad ID:
Farm/Lease Name: GAIS 1
License Status: ACTIVE
Spud Date: 2005-08-02
Permit Date: 2005-02-15
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.532763
Longitude: -79.425085

For data sources see[1][2][3]

Well History

Date Event
2005-02-15 New Permit Application
2005-08-02 Performed Spud Operation
2005-08-08 Drilling Completion
2005-08-16 Perforation
2006-05-04 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 US ENERGY EXPLORATION CORP 457 30 0.00 0 0.00 0
2008 US ENERGY EXPLORATION CORP 3065.00 360 0.00 0 0.00 0
2009 US ENERGY EXPLORATION CORP 2287.00 360 0.00 0 0.00 0
2010 US ENERGY EXPLORATION CORP 1,838.00 360 0.00 0 0.00 0
2011 US ENERGY EXPLORATION CORP 1,261.00 360 0.00 0 0.00 0
2012 US ENERGY EXPLORATION CORP 1,050.00 360 0.00 0 0.00 0
2013 US ENERGY EXPLORATION CORP 728.00 360 0.00 0 0.00 0
2014 US ENERGY EXPLORATION CORP 753.00 365 0.00 0 0.00 0
2015 US ENERGY EXPLORATION CORP 545.00 365 0.00 0 0.00 0
2016 US ENERGY EXPLORATION CORP 359.00 330 0.00 0 0.00 0
2017 US ENERGY EXPLORATION CORP 296.00 134 0.00 0 0.00 0
2018 US ENERGY EXPLORATION CORP 759.00 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1883555 Primary Facility 2010-05-07 Routine/Complete Inspection No Violations Noted Based on record, permit was approved on 2/15//05. Well installed on 8/8/05 to a depth of 4320 ft. Report submitted and approved on 4/6/06. Well completed with 8¿ pipe reduced to 4 ¿pipe reduced to 2¿ production pipe and multiple shut off valves. Production equipment consists of heater, separator (180 psi), 100 bbl (45 bbl) and dual phase data logger (170 psi/0 psi). At the time of inspection, no IW or E&S issues at the site. No signs of fluid or gas leakage around well head. Well tag was present.

For data sources see[6]

References