X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-083-49911

Well Details

Well ID: 37-083-49911
Loading map...
Country: United States
State: Pennsylvania
County: McKean
Municipality: Hamilton Township
Operator Name: DIVERSIFIED OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: LOT 90 90 5
License Status: ACTIVE
Spud Date:
Permit Date: 2004-09-29
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.775194
Longitude: -78.933889

For data sources see[1][2][3]

Well History

Date Event
2004-09-29 New Permit Application
2005-02-10 Performed Spud Operation
2005-02-11 Drilling Completion
2005-06-07 Perforation
2005-10-13 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 ATLAS RESOURCES INC 0.00 0 0.00 0 0.00 0
2006 ATLAS RESOURCES INC 0.00 0 0.00 0 0.00 0
2007 M & M ROYALTY LTD 0.00 0 0.00 0 0.00 0
2008 ATLAS RESOURCES LLC 753.00 366 0.00 0 0.00 0
2009 ATLAS RESOURCES LLC 411.00 365 0.00 0 0.00 0
2010 ATLAS RESOURCES LLC 104.00 365 0.00 0 0.00 0
2011 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2012 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2013 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2014 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2015 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2016 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2017 ATLAS RESOURCES LLC 0.00 0 0.00 0 0.00 0
2018 DIVERSIFIED OIL & GAS LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2005 M & M ROYALTY LTD Brine 1,400.00 Bbl Brine or Industrial Waste Treatment Plt PA0102784

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1437372 Primary Facility 2005-04-07 Routine/Complete Inspection No Violations Noted
1642492 Primary Facility 2007-08-06 Routine/Complete Inspection No Violations Noted
1977208 Primary Facility 2011-05-31 Routine/Complete Inspection No Violations Noted
2413023 Primary Facility 2015-09-15 Routine/Complete Inspection No Violations Noted
2808067 Primary Facility 2018-11-29 Routine/Complete Inspection Violation(s) Noted This is a combination well with a pumpjack attached. The gas motor has been removed from the jack, and the belt is missing. The valves appear to be shut. Gas can be heard coming out of the wellhead. Trees are growing up around the pumpjack from lack of maintenance. There is a tank battery associated with this well on the main access road; brush and trees fill the area within containment and the separators and gas meter box are rusted with paint falling off. The gas meter chart has not been changed since 1-29-16. There was no production reported for this well on the 2017 annual production report - comments provided in the report indicate “Well Temporarily Not Producing”.

This well is abandoned as defined in section 3203 of the 2012 Oil & Gas Act.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2808067 834476 2018-11-29 2019-03-07 OGA3220(A) Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
834476 369710 NOV - Notice of Violation 2019-03-07
834476 372946 COA - Consent Order and Agreement

For data sources see[7]

References