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37-117-21148

Well Details

Well ID: 37-117-21148
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Country: United States
State: Pennsylvania
County: Tioga
Municipality: Duncan Township
Operator Name: EQT PROD CO
Well Pad ID: 149046
Farm/Lease Name: PHOENIX 590934
License Status:
Spud Date:
Permit Date: 2011-01-12
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 41.645747
Longitude: -77.256094

For data sources see[1][2][3]

Well History

Date Event
2011-01-12 New Permit Application
2011-11-15 Performed Spud Operation
2011-12-21 New Permit Application
2012-03-10 Drilling Completion
2012-05-09 Perforation
2013-12-09 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2012-05-12 2012-05-12 7,763 5,862,276

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 FR-66 Friction Reducer Halliburton Energy Services Friction Reducer Distillates, petroleum, hydrotreated light 64742-47-8 30.00 0.03
Hydrochloric Acid Halliburton Energy Services 15 HCl Acid Hydrochloric acid 7647-01-0 28.00 0.02
Methanol 67-56-1 60.00 0.00025000
BA-40L Halliburton Energy Services Buffer Carbonic acid, dipotassium salt 584-08-7 60.00 0.00514000
GBW-30 BREAKER Halliburton Energy Services Enzyme Breaker Hemicellulase enzyme 9012-54-8 15.00 0.00
Hydrochloric Acid Halliburton Energy Services Corrosion Inhibitor Propargyl alcohol 107-19-7 10.00 0.00004000
LGC-36 Halliburton Energy Services Gelling Agent Guar gum 9000-30-0 30.00 0.00113000
Naphtha, petroleum, hydrotreated heavy 64742-48-9 30.00 0.00113000
LP-65 Halliburton Energy Services Scale Inhibitor Ammonium chloride 12125-02-9 10.00 0.00275000
BE-9 Biocide Halliburton Energy Services Biocide Tri-n-butyl tetradecyl phosphonium chloride 81741-28-8 10.00 0.00454000
SP Breaker Halliburton Energy Services Oxidizing Breaker Sodium persulfate 7775-27-1 100.00 0.00010000

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 EQT PROD CO 0.00 0 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0
2012 EQT PROD CO 254,656.00 166 0.00 0 0.00 0
2013 EQT PROD CO 346,220.00 365 0.00 0 0.00 0
2014 EQT PROD CO 278,665.00 365 0.00 0 0.00 0
2015 EQT PROD CO 120,404.00 265 0.00 0 0.00 0
2016 EQT PROD CO 231,214.00 364 0.00 0 0.00 0
2017 EQT PROD CO 107,981.00 267 0.00 0 0.00 0
2018 EQT PROD CO 94,263.00 239 0.00 0 0.00 0
2019 EQT PROD CO 179,167.00 312 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 EQT PROD CO Produced Fluid 784.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2012 EQT PROD CO Produced Fluid 419.00 Bbl INJECTION DISPOSAL WELL 34-155-21447
2012 EQT PROD CO Produced Fluid 12,974.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2012 EQT PROD CO Drilling Fluid Waste 110.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2012 EQT PROD CO Produced Fluid 1,351.00 Bbl INJECTION DISPOSAL WELL 34-083-24137
2012 EQT PROD CO Produced Fluid 802.00 Bbl REUSE OTHER THAN ROAD SPREADING
2012 EQT PROD CO Drilling Fluid Waste 440.00 Bbl REUSE OTHER THAN ROAD SPREADING
2012 EQT PROD CO Produced Fluid 10,121.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123
2012 EQT PROD CO Fracing Fluid Waste 24,983.00 Bbl REUSE OTHER THAN ROAD SPREADING
2012 EQT PROD CO Fracing Fluid Waste 260.00 Bbl INJECTION DISPOSAL WELL 34-007-24355
2012 EQT PROD CO Produced Fluid 579.00 Bbl INJECTION DISPOSAL WELL 34-155-21438
2012 EQT PROD CO Fracing Fluid Waste 23,326.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2012 EQT PROD CO Fracing Fluid Waste 240.00 Bbl INJECTION DISPOSAL WELL 34-083-24137
2012 EQT PROD CO Fracing Fluid Waste 3,511.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123
2013 EQT PROD CO Produced Fluid 11,866.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 EQT PROD CO Fracing Fluid Waste 100.00 Bbl INJECTION DISPOSAL WELL 34-155-23223
2013 EQT PROD CO Fracing Fluid Waste 107.00 Bbl INJECTION DISPOSAL WELL 34-155-21438
2013 EQT PROD CO Produced Fluid 2,240.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2013 EQT PROD CO Fracing Fluid Waste 61.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2013 EQT PROD CO Fracing Fluid Waste 46,098.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 EQT PROD CO Produced Fluid 2,096.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2013 EQT PROD CO Produced Fluid 1,438.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123
2013 EQT PROD CO Produced Fluid 101.00 Bbl INJECTION DISPOSAL WELL 34-155-21438
2013 EQT PROD CO Produced Fluid 264.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC018
2013 EQT PROD CO Produced Fluid 293.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123SW018
2014 EQT PROD CO Fracing Fluid Waste 110.00 Bbl REUSE OTHER THAN ROAD SPREADING
2014 EQT PROD CO Produced Fluid 6,179.00 Bbl REUSE OTHER THAN ROAD SPREADING
2014 EQT PROD CO Produced Fluid 2,130.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2015 EQT PROD CO Produced Fluid 228.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NW011
2015 EQT PROD CO Produced Fluid 200.00 Bbl INJECTION DISPOSAL WELL 34-007-2-3097
2015 EQT PROD CO Produced Fluid 8.00 Bbl INJECTION DISPOSAL WELL 34-007-21847
2015 EQT PROD CO Fracing Fluid Waste 1,320.00 Bbl REUSE OTHER THAN ROAD SPREADING
2015 EQT PROD CO Produced Fluid 1,691.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 EQT PROD CO Produced Fluid 693.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2016 EQT PROD CO Produced Fluid 507.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NW011
2016 EQT PROD CO Produced Fluid 200.00 Bbl REUSE OTHER THAN ROAD SPREADING
2017 EQT PROD CO Produced Fluid 969.86 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2017 EQT PROD CO Other Oil & Gas Wastes 109.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2017 EQT PROD CO Produced Fluid 270.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2017 EQT PROD CO Other Oil & Gas Wastes 270.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2017 EQT PROD CO Produced Fluid 360.00 Bbl REUSE (AT WELL PAD)
2018 EQT PROD CO Produced Fluid 954.58 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2018 EQT PROD CO Other Oil & Gas Wastes 584.82 Bbl REUSE (AT WELL PAD)
2018 EQT PROD CO Other Oil & Gas Wastes 73.64 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW009
2018 EQT PROD CO Other Oil & Gas Wastes 1,002.99 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2018 EQT PROD CO Produced Fluid 32.42 Bbl REUSE (AT WELL PAD)
2018 EQT PROD CO Other Oil & Gas Wastes 27.28 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2018 EQT PROD CO Other Oil & Gas Wastes 47.27 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2018 EQT PROD CO Other Oil & Gas Wastes 5.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 EQT PROD CO Other Oil & Gas Wastes 1,213.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2018 EQT PROD CO Produced Fluid 37.95 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2018 EQT PROD CO Produced Fluid 330.04 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2018 EQT PROD CO Produced Fluid 3.48 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 EQT PROD CO Produced Fluid 986.55 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2018 EQT PROD CO Produced Fluid 111.37 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW009
2019 EQT PROD CO Produced Fluid 19.58 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW009
2019 EQT PROD CO Other Oil & Gas Wastes 11.82 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2019 EQT PROD CO Produced Fluid 85.57 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2019 EQT PROD CO Other Oil & Gas Wastes 20.45 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2019 EQT PROD CO Other Oil & Gas Wastes 486.27 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2019 EQT PROD CO Produced Fluid 855.65 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2019 EQT PROD CO Produced Fluid 631.98 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2019 EQT PROD CO Other Oil & Gas Wastes 25.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW009
2019 EQT PROD CO Other Oil & Gas Wastes 50.45 Bbl REUSE (AT WELL PAD)
2019 EQT PROD CO Produced Fluid 1,188.45 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2019 EQT PROD CO Produced Fluid 13.54 Bbl REUSE (AT WELL PAD)

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2028267 Primary Facility 2011-12-20 Drilling/Alteration No Violations Noted
2030310 Primary Facility 2011-12-20 Routine/Complete Inspection No Violations Noted
2034357 Primary Facility 2012-01-11 Routine/Complete Inspection No Violations Noted
2066392 Primary Facility 2012-05-09 Drilling/Alteration No Violations Noted Inspection conducted on Pad S well site. WQS also conducting inspection on Pad S Impoundment area following reported flowback spill (300-500 gallons reported).
2067209 Primary Facility 2012-05-09 Incident- Response to Accident or Event Violation(s) Noted
2067590 Primary Facility 2012-05-10 Follow-up Inspection Outstanding Violations - No Viols Req'd 5/10/12 FUI insp to verify clean up status of 5/8/12 flowback spill. TLT
2074218 Primary Facility 2012-05-31 Incident- Response to Accident or Event Violation(s) Noted 5-31-12 incident inspection following notification of high conductivity in surface water (spring) and potential leaking impoundment. TLT
2074292 Primary Facility 2012-06-01 Follow-up Inspection Outstanding Violations - No Viols Req'd 6/1/12 FUI inspection to field screen/monitor release. TLT
2075700 Primary Facility 2012-06-07 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1100 hours on June 7, 2012. The purpose of this visit was to evaluate the status of flowback removal from Impoundment 2 and to identify the extent of an elevated reading of specific conductance discovered earlier in the week.
2075838 Primary Facility 2012-06-04 Follow-up Inspection Outstanding Violations - No Viols Req'd FUI Inspection to evaluate impoundment drawdown and conduct additional field screening. TLT
2076502 Primary Facility 2012-06-05 Follow-up Inspection Outstanding Violations - No Viols Req'd The "northeast spring" (41° 39' 01"N, 77° 15' 12"W) = >19,999 uS/cm
2076601 Primary Facility 2012-06-06 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site from approximately 1045hours to 1500 hours on June 6, 2012. Representatives of the Department included Terra Tokarz (Water Quality Specialist), Jessica Ritenour (Professional Geologist ), Randy Farmeri (Professional Geologist Manager) and myself . Steve Kepler (Fisheries Biologist) and Heather Smiles (Fisheries Biologist) from the PA Fish and Boat Commission (PA F&BC ), were also present. Dave Allison and Mike Cromley from EQT were on-site.
2076602 Primary Facility 2012-06-13 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1015 hours on June 13, 2012. The purpose of this visit was to evaluate the status of flowback removal from Impoundment 2, to identify the extent of an elevated reading of specific conductance discovered during previous inspections and to establish routine sampling points.
2076668 Primary Facility 2012-05-30 Follow-up Inspection Outstanding Violations - No Viols Req'd
2076733 Primary Facility 2012-06-08 Follow-up Inspection Outstanding Violations - No Viols Req'd
2076919 Primary Facility 2012-06-11 Follow-up Inspection Violation(s) & Outstanding Violations
2077276 Primary Facility 2012-06-12 Follow-up Inspection Outstanding Violations - No Viols Req'd
2077279 Primary Facility 2012-06-19 Follow-up Inspection Outstanding Violations - No Viols Req'd
2077314 Primary Facility 2012-06-20 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 0930 hours on June 20, 2012. The purpose of this visit was to document readings of specific conductance noted during previous inspections and conducting routine sample collection.
2078900 Primary Facility 2012-06-22 Follow-up Inspection Outstanding Violations - No Viols Req'd
2079004 Primary Facility 2012-06-26 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1200 hours on June 26, 2012. The purpose of this visit was to document readings of specific conductance noted during previous inspections and conducting routine sample collection.
2081425 Primary Facility 2012-07-05 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1000 hours on July 5, 2012. The purpose of this visit was to document readings of specific conductance noted during previous inspections and conducting routine sample collection. The well pad area was not inspected at this time. Violations cited on 5/31/12 and 6/19/12 remain outstanding, no new violations were cited during this inspection. -MRN
2081849 Primary Facility 2012-07-02 Follow-up Inspection Outstanding Violations - No Viols Req'd
2082796 Primary Facility 2012-07-12 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1200 hours to 1500 on July 12, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection at the location noted below.
2083599 Primary Facility 2012-07-16 Follow-up Inspection Outstanding Violations - No Viols Req'd
2085691 Primary Facility 2012-07-18 Follow-up Inspection Outstanding Violations - No Viols Req'd
2085900 Primary Facility 2012-07-19 Follow-up Inspection Outstanding Violations - No Viols Req'd
2086157 Primary Facility 2012-07-25 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1230 hours to 1415 on July 25, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection at the location noted below.
2086416 Primary Facility 2012-07-23 Follow-up Inspection Outstanding Violations - No Viols Req'd
2088545 Primary Facility 2012-08-02 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1200 hours to 1415 on August 2, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection. The well pad area was not inspected at this time. Violations cited on 5/31/12 and 6/19/12 remain outstanding, no new violations were cited during this inspection. - MRN
2089841 Primary Facility 2012-07-30 Follow-up Inspection Outstanding Violations - No Viols Req'd
2090037 Primary Facility 2012-08-02 Follow-up Inspection Outstanding Violations - No Viols Req'd
2090399 Primary Facility 2012-08-09 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1045 hours to 1330 on August 9, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection - MRN
2091888 Primary Facility 2012-08-09 Follow-up Inspection Violation(s) & Outstanding Violations
2092223 Primary Facility 2012-08-16 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1220 hours to 1420 on August 16, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection
2095754 Primary Facility 2012-08-23 Follow-up Inspection Outstanding Violations - No Viols Req'd
2096381 Primary Facility 2012-08-30 Follow-up Inspection Outstanding Violations - No Viols Req'd
2097928 Primary Facility 2012-09-05 Follow-up Inspection Outstanding Violations - No Viols Req'd
2099760 Primary Facility 2012-09-13 Follow-up Inspection Outstanding Violations - No Viols Req'd
2101580 Primary Facility 2012-09-20 Follow-up Inspection Outstanding Violations - No Viols Req'd
2103263 Primary Facility 2012-09-26 Follow-up Inspection Violation(s) & Outstanding Violations
2105375 Primary Facility 2012-10-04 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1300 hours to 1500 on October 4, 2012. The purpose of this visit was to document readings of specific conductance and to conduct routine sample collection. The well pad area was not inspected at this time. Violations cited on 5/31/12 and 6/19/12 remain outstanding, no new violations were cited during this inspection. - MRN
2107788 Primary Facility 2012-10-16 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1300 hours to 1400 on October 16, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection. The well pad area was not inspected at this time. Violations cited on 5/31/12 and 6/19/12 remain outstanding, no new violations were cited during this inspection. - MRN
2112105 Primary Facility 2012-11-01 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1200 hours to 1330 on November 1, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection. - MRN
2116114 Primary Facility 2012-11-15 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 0800 hours to 1055 on November 15, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection. - MRN
2123452 Primary Facility 2012-12-13 Follow-up Inspection Outstanding Violations - No Viols Req'd A follow up inspection was conducted at the EQT Pad S Flowback Impoundment 2 site at approximately 1200 hours to 1420 on December 13, 2012. The purpose of this visit was to document readings of specific conductance and conducting routine sample collection. - MRN
2135695 Primary Facility 2013-01-29 Follow-up Inspection Outstanding Violations - No Viols Req'd
2153293 Primary Facility 2013-04-01 Follow-up Inspection Outstanding Violations - No Viols Req'd
2155213 Primary Facility 2013-04-05 Incident- Response to Accident or Event Outstanding Violations - No Viols Req'd 90 bbl spill of recovered water from Pad S impoundment. 20 bbls outside of containment. Conductivity of fluid was around 1300 uS/cm. TLT
2170636 Primary Facility 2013-05-23 Follow-up Inspection Outstanding Violations - No Viols Req'd
2175711 Primary Facility 2013-06-10 Follow-up Inspection Outstanding Violations - No Viols Req'd
2176811 Primary Facility 2013-06-14 Follow-up Inspection Outstanding Violations - No Viols Req'd
2177337 Primary Facility 2013-06-19 Follow-up Inspection Outstanding Violations - No Viols Req'd FUI Insp. Impoundment being reclaimed. Work started 6/17/13. TLT
2180763 Primary Facility 2013-06-28 Follow-up Inspection Outstanding Violations - No Viols Req'd
2185841 Primary Facility 2013-07-17 Follow-up Inspection Outstanding Violations - No Viols Req'd
2196806 Primary Facility 2013-08-14 Follow-up Inspection Outstanding Violations - No Viols Req'd
2199756 Primary Facility 2013-08-28 Follow-up Inspection Outstanding Violations - No Viols Req'd
2230356 Primary Facility 2013-11-05 Routine/Complete Inspection No Violations Noted
2254825 Primary Facility 2014-02-27 Follow-up Inspection No Violations Noted
2262630 Primary Facility 2014-04-14 Follow-up Inspection Outstanding Violations - No Viols Req'd
2326237 Primary Facility 2014-11-24 Follow-up Inspection Outstanding Violations - No Viols Req'd Follow up inspection to conduct routine monitoring and sampling. TLT
2482795 Primary Facility 2016-05-09 Follow-up Inspection Outstanding Violations - No Viols Req'd Follow up inspection to collect samples from monitoring locations. TLT
2556980 Primary Facility 2017-01-25 Follow-up Inspection Outstanding Violations - Viols Req'd Follow up inspection. The violations cited on 5/8/12, 5/31/12, 6/11/12, 8/9/12 and 9/26/12 are outstanding. No new violations cited during this inspection. TLT
2601414 Primary Facility 2017-06-06 Routine/Complete Inspection No Violations Noted I arrived on-site @ 09:35 hrs. and met Bill Wallace of EQT. Patterson UTI rig 294 on location tripping into the 593851 well. Some housekeeping issues noted, all in containment and mostly related to precipitation; Mr. Wallace informed me that a vac truck was en route. I noted 2 spots where the primary containment may have been allowing rainwater through to the pad; Mr. Wallace was aware of one of the spots, and will have both checked and/ or repaired. I departed the site @ 10:20 hrs.
2613896 Primary Facility 2017-07-06 Routine/Complete Inspection No Violations Noted I arrived on-site and met Bill Wallace, EQT company man. Patterson UTI rig #294 on location. Bill informed me that they had just started drilling on the 593853 well ( permit #117-21786). He also told me that after my last inspection in which I identified some spots where the pad containment appeared to be leaking that they had wound up moving the rig off the site, pulling up the rig mats, and replacing the pad-wide containment due to issues with the liner system. The new liner was in good shape and appeared to be a heavier, thicker material. The pad was in good condition overall, with no issues noted.
2660398 Primary Facility 2017-11-12 Incident- Response to Accident or Event No Violations Noted Rich Herbstritt (DEP, OGI) and I inspected this site after EQT reported loss of well control on one of the three Marcellus wells FTS (contractor) was hydraulically fracturing ("zipperfrack"). We spoke with EQT's VP of drilling/ completions on site, Jim Helmick, who explained the following: last night at ~2330 hrs, the Cactus (brandname) well head began to leak flowback and methane while FTS was fracturing. Between then and noon today, vacuum trucks have been removing the flowback liquid and delivering it to 3 locations: Hydrorecovery in Antrim, PA, a Seneca Resources site, and to an Above-ground Storage Tank (AST). They estimate vac trucks removed 1,900 barrels between 2330 and noon, and that the well is still releasing ~110 barrels/hr (~1 vac truck load/hr) into the cellar. Vac trucks have been able to keep up with removal of liquid from the cellar, preventing overflows. Wild Well Control out of Texas has personnel on site who are addressing the well control issue. Wild Well reportedly got an LEL re
2678477 Primary Facility 2018-01-04 Routine/Complete Inspection Outstanding Violations - Viols Req'd The Department of Environmental Protection (DEP) inspected the EQT Phoenix pad S located in Duncan Township, Tioga County on January 4, 2018 at 11:30 hrs. The weather was 17 degrees. Overcast with 3 inches of snow on the ground. 17 mph winds out of the NW. Humidity 67%. Pressure 29.7 inHg.

There was no activity onsite during the inspection. Pad wide containment and rig matting appears to still be in place beneath the snow cover. Two residual waste vac trucks are parked onsite. The previous inspection noted the Phoenix 593850-593855 wells were drilled Jan.-July 2017; stimulation notices were received in September. The previous inspection conducted in Oct. noted the wells were being drilled out and flowed back. No issues were noted on the pad.

The Above ground Storage Tank (AST) located across the access road from pad S is labeled "impaired water only". Trucks were observed idling on containment. No visible staining or fluid was observed in the area adjacent to the AST.

The Phoenix 590934 (117-21148) May 31

2745935 Primary Facility 2018-06-19 Routine/Complete Inspection Outstanding Violations - Viols Req'd The DEP inspected the EQT-Phoenix Pad S located in Duncan Twp, Tioga Co. on 6/19/2018 @1300 hours. The weather was 78 degrees, 45% humidity and winds N 12mph. Mike Cromley, EQT Env Coordinator and Stan Bridges, EQT Company Man were present during the inspection. The well site is currently set up for flowback.

I observed the well pad and water storage pad. The Phoenix 593850-593855 wells were drilled Jan.-July 2017; stimulation notices were received in April for the 593853-593855. As of today's inspection, EQT was completing flow back of the 59383-593855 wells.

Well pad containment consists of bermed, pad-wide containment with mats on top. Mats in some areas were broken down, in need of repair, showing the containment underneath. Localized containment structures were observed under individual pieces of

Violations against API#117-21148 remain OUTSTANDING. Please address any deficiencies and contact me with any questions.

I departed the site at 1500 hours.

2808128 Primary Facility 2018-11-28 Routine/Complete Inspection Outstanding Violations - Viols Req'd The DEP conducted a ROUTINE inspection of the EQT - Phoenix Pad S located in Duncan Twp, Tioga Co. on 11/28/2018 @1300 hours. The weather was cloudy/light snow 31 degrees, Humidity 71%, Winds WNW 19 mph. Two Beimel trucks were onsite emptying fluid from the production tanks onsite.

The Phoenix 593850-593855 wells were drilled Jan.-July 2017; stimulation notices were received in April for the 593853-593855. In June of 2018 EQT completed flow back of the 59383-593855 wells. As of today's inspection, the pad is setup for production.

No areas of elevated conductivity were located on the pad surface. Perimeter E&S controls appeared to be functioning. Violations against the Phoenix 590934 API#117-21148 remain OUTSTANDING.

2845408 Primary Facility 2019-02-26 Routine/Complete Inspection No Violations Noted I arrived onsite to meet with Doug Oberdorf of EQT. One EWS evaporator was present on the pad, but had not yet been hooked up to the production tanks or placed in containment. Gregg Johnson of EWW was also present. Gregg informed me that high winds on Monday had caused them to postpone placement of the evaporator unit. The OG71A for the site called for 3 evaporator units; Gregg informed me that the trial would begin with 1 unit, and the other 2 would be added in later. The production tank containment appeared to be in good condition, with less than 2" of ice. Several of the well cellars had water in them within 2' of the top; I recommend that these be monitored and vacced out before overtopping.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2067209 639194 05/08/2012 2012-05-08 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances. Administrative 78.56(a)
2067209 639195 05/08/2012 2012-05-08 SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. Environmental Health & Safety
2067209 639196 05/08/2012 2012-05-08 CSL402POTPOL - There is a potential for polluting substance(s) reaching Waters of the Commonwealth and may require a permit Environmental Health & Safety
2074218 641131 05/31/2012 2012-05-31 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances. Administrative 78.56(a) for failure to contain a pollutional substance in a pit, tank or series of pits and tanks. High conductivity readings recorded in spring located near an impoundment used to contain flowback. TLT
2074218 641132 05/31/2012 2012-05-31 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt Environmental Health & Safety 691.301 of CSL for discharging an industrial waste to Waters of the Commonwealth. High conductivity readings recorded in spring located near impoundment containing flowback fluid. TLT
2074218 641133 05/31/2012 2012-05-31 307CSL - Discharge of industrial waste to waters of Commonwealth without a permit. Environmental Health & Safety 691.307 of the CSL for causing or allowing an unpermitted discharge of an industrial waste into Waters of the Commonwealth. High conductivity readings recorded in a spring located near and downgradient of an impoundment containing flowback fluid. TLT
2074218 641134 05/31/2012 2012-05-31 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety 691.401 of the CSL for allowing an unlawful discharge of a pollutional substance to Waters of the Commonwealth. High conductivity readings recorded in a spring located near and down gradient from an impoundment containing flowback fluid. TLT
2074218 641135 05/31/2012 2012-05-31 SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. Environmental Health & Safety 6018.301 of the SWMA for an unpermitted discharge of residual waste onto the ground. High conductivity readings recorded in spring discharge located near and down gradient from an impoundment containing flowback fluid. TLT
2076919 642081 06/11/2012 2012-06-11 78.56PITCNST - Impoundment not structurally sound, impermeable, 3rd party protected, greater than 20" of seasonal high ground water table Administrative Operator failed to maintain an impermeable pit containing a pollutional substance
2076919 642082 06/11/2012 2012-06-11 78.56(3) - Impoundment not structurally sound, impermeable, 3rd party protected. Administrative 78.56(a)(4)(iv) - After the liner was determined to be torn or otherwise lost its integrity, the operator failed to manage the pit to prevent the pits contents form leaking from the pit.
2076919 642083 06/11/2012 2012-06-11 91.34A - Failure to take all necessary measures to prevent spill. Inadequate diking, potential pollution Environmental Health & Safety Persons engaged in an activity which includes the impoundment, production, processing, transportation, storage, use, application or disposal of pollutants shall take necessary measures to prevent the substances from reaching Waters of the Commonwealth
2091888 646771 08/09/2012 2012-08-09 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. Environmental Health & Safety 78.54 for failure to control/dispose fluids in a manner that prevents pollution to waters of the Commonwealth. Pollutional substance discharging off liner onto the ground. TLT
2091888 646772 08/09/2012 2012-08-09 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt Environmental Health & Safety 691.301 CSL. Operator allowed discharge of industrial waste to waters of the Commonwealth. Wetland near east corner of well pad had high conductivity and elevated chloride concentration. TLT
2091888 646773 08/09/2012 2012-08-09 307CSL - Discharge of industrial waste to waters of Commonwealth without a permit. Environmental Health & Safety 691.307 CSL. Operator allowed an unpermitted discharge of industrial waste into waters of the Commonwealth. Wetland near east corner of well pad had high conductivity and elevated chloride concentration. TLT
2091888 646774 08/09/2012 2012-08-09 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety 691.401 CSL. Operator allowed an unlawful discharge of a pollutional substance to waters of the Commonwealth. Wetland near east corner of well pad had high conductivity and elevated chloride concentration. TLT
2091888 646775 08/09/2012 2012-08-09 SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. Environmental Health & Safety 6018.301 SWMA. Operator allowed an unpermitted discharge of residual waste on to the ground. Pollutional substance discharging off liner onto the ground. TLT
2103263 650280 09/26/2012 2012-09-26 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. Environmental Health & Safety 78.54. Department sample results show elevated concentrations of chloride, sulfate and strontium from well pad sump discharge. TLT
2103263 650281 09/26/2012 2012-09-26 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. Environmental Health & Safety CSL 402 for potential to pollute Waters of the Commonwealth. Department sample results show well pad sump discharge had elevated concentrations of chloride, sulfate and strontium. TLT
2103263 650282 09/26/2012 2012-09-26 SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. Environmental Health & Safety SWMA 301 for an unpermitted discharge of residual waste onto the ground. Well pad sump observed discharging onto ground. Department sample results show elevated concentrations of chloride, sulfate and strontium. TLT
2556980 777578 2017-01-25 2019-01-11 78a56(a) Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2556980 777579 2017-01-25 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2556980 777580 2017-01-25 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2556980 777581 2017-01-25 2018-11-09 78a56(a) Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2556980 777582 2017-01-25 2018-11-09 CSL 301 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2556980 777583 2017-01-25 2018-11-09 CSL 307(a) Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2556980 777584 2017-01-25 2018-11-09 CSL 401 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2556980 777585 2017-01-25 2018-11-09 SWMA 301 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2556980 777586 2017-01-25 2018-11-09 78.56(a)4i Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919). TLT
2556980 777587 2017-01-25 2018-11-09 78.56(a)4iv Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919). TLT
2556980 777588 2017-01-25 2018-11-09 91.34(A) Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919). TLT
2556980 777589 2017-01-25 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

CACP Enf. ID 371337

2556980 777590 2017-01-25 2019-01-11 CSL 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

CACP Enf. ID 371337

2556980 777591 2017-01-25 2019-01-11 CSL 307(a) Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

CACP Enf. ID 371337

2556980 777592 2017-01-25 2019-01-11 CSL 401 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

CACP Enf. ID 371337

2556980 777593 2017-01-25 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

CACP Enf. ID 371337

2556980 777594 2017-01-25 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT

CACP Enf. ID 371337

2556980 777595 2017-01-25 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT

CACP Enf. ID 371337

2556980 777596 2017-01-25 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT

CACP Enf. ID 371337

2678477 805308 2018-01-04 2018-11-09 CSL 301 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218).
2678477 805309 2018-01-04 2019-01-11 CSL 307(a) Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888).
2678477 805310 2018-01-04 2018-11-09 91.34(A) Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919).
2678477 805311 2018-01-04 2019-01-11 CSL 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888).
2678477 805312 2018-01-04 2019-01-11 CSL 401 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888).
2678477 805313 2018-01-04 2018-11-09 CSL 307(a) Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218).
2678477 805314 2018-01-04 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263).
2678477 805315 2018-01-04 2018-11-09 CSL 401 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218).
2678477 805316 2018-01-04 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 5/9/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information.

CACP Enf. ID 371337

2678477 805317 2018-01-04 2018-11-09 78.56(a)4i Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919).
2678477 805318 2018-01-04 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263).
2678477 805319 2018-01-04 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263).
2678477 805320 2018-01-04 2018-11-09 SWMA 301 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218).
2678477 805321 2018-01-04 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888).
2678477 805322 2018-01-04 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888).
2678477 805323 2018-01-04 2018-11-09 78.56(a)4iv Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919).
2678477 805324 2018-01-04 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 5/9/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information.

CACP Enf. ID 371337

2678477 805325 2018-01-04 2019-01-11 78a56(a) Environmental Health & Safety Open violation cited on 5/9/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2678477 805326 2018-01-04 2018-11-09 78a56(a) Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218).
2745935 820754 2018-06-19 2019-01-11 78a56(a) Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2745935 820755 2018-06-19 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2745935 820756 2018-06-19 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

CACP Enf. ID 371337

2745935 820757 2018-06-19 2018-11-09 78a56(a) Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2745935 820758 2018-06-19 2018-11-09 CSL 301 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2745935 820759 2018-06-19 2018-11-09 CSL 307(a) Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2745935 820760 2018-06-19 2018-11-09 CSL 401 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2745935 820761 2018-06-19 2018-11-09 SWMA 301 Environmental Health & Safety Outstanding violation cited on 5/31/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 5/31/12 inspection report (#2074218). TLT
2745935 820762 2018-06-19 2018-11-09 78.56(a)4i Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919). TLT
2745935 820763 2018-06-19 2018-11-09 78.56(a)4iv Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919). TLT
2745935 820764 2018-06-19 2018-11-09 91.34(A) Environmental Health & Safety Outstanding violation cited on 6/11/12 associated with a release of produced water from the Phoenix Pad S pit. For additional information, see the 6/11/12 inspection report (#2076919). TLT
2745935 820765 2018-06-19 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT
2745935 820766 2018-06-19 2019-01-11 CSL 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT
2745935 820767 2018-06-19 2019-01-11 CSL 307(a) Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT
2745935 820768 2018-06-19 2019-01-11 CSL 401 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT
2745935 820769 2018-06-19 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT
2745935 820770 2018-06-19 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT
2745935 820771 2018-06-19 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT
2745935 820772 2018-06-19 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT
2808128 834508 2018-11-28 2019-01-11 78a56(a) Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

This violation was originally cited in an inspection report dated 5/9/2012

2808128 834509 2018-11-28 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

This violation was originally cited in an inspection report dated 5/9/2012

2808128 834510 2018-11-28 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 5/8/12 associated with a flowback release from a temporary transfer line. See the 5/9/12 inspection report (#2067209) for additional information. TLT

This violation was originally cited in an inspection report dated 5/9/2012

2808128 834511 2018-11-28 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

This violation was originally cited in an inspection report dated 8/9/2012

2808128 834512 2018-11-28 2019-01-11 CSL 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

This violation was originally cited in an inspection report dated 8/9/2012

2808128 834513 2018-11-28 2019-01-11 CSL 307(a) Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

This violation was originally cited in an inspection report dated 8/9/2012

2808128 834514 2018-11-28 2019-01-11 CSL 401 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

This violation was originally cited in an inspection report dated 8/9/2012

2808128 834515 2018-11-28 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 8/9/12 associated with a release of flowback fluid off of containment onto the pad surface at Phoenix Pad S. For additional information, see the 8/9/12 inspection report (#2091888). TLT

This violation was originally cited in an inspection report dated 8/9/2012

2808128 834516 2018-11-28 2019-01-11 78a54 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT

This violation was originally cited in an inspection report dated 9/26/2012

2808128 834517 2018-11-28 2019-01-11 CSL 402(b) Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT

This violation was originally cited in an inspection report dated 9/26/2012

2808128 834518 2018-11-28 2019-01-11 SWMA 301 Environmental Health & Safety Open violation cited on 9/26/12 associated with a sump discharge of a pollutional material at Phoenix Pad S. For additional information, see the 9/26/12 inspection report (#2103263). TLT

This violation was originally cited in an inspection report dated 9/26/2012

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
639194 283701 NOV - Notice of Violation
639194 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
639195 283701 NOV - Notice of Violation
639195 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
639196 283701 NOV - Notice of Violation
639196 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
641131 284604 NOV - Notice of Violation
641132 284604 NOV - Notice of Violation
641132 369303 EHBO - Environmental Hearing Board Order Administrative Close Out 2018-11-06 2018-11-09 $1,137,296.00 $1,137,296.00
641133 284604 NOV - Notice of Violation
641133 369303 EHBO - Environmental Hearing Board Order Administrative Close Out 2018-11-06 2018-11-09 $1,137,296.00 $1,137,296.00
641134 284604 NOV - Notice of Violation
641134 369303 EHBO - Environmental Hearing Board Order Administrative Close Out 2018-11-06 2018-11-09 $1,137,296.00 $1,137,296.00
641135 284604 NOV - Notice of Violation
642081 285126 NOV - Notice of Violation
642082 285126 NOV - Notice of Violation
642083 285126 NOV - Notice of Violation
642083 369303 EHBO - Environmental Hearing Board Order Administrative Close Out 2018-11-06 2018-11-09 $1,137,296.00 $1,137,296.00
646771 287421 NOV - Notice of Violation
646771 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
646772 287421 NOV - Notice of Violation
646772 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
646773 287421 NOV - Notice of Violation
646773 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
646774 287421 NOV - Notice of Violation
646774 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
646775 287421 NOV - Notice of Violation
646775 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
650280 289007 NOV - Notice of Violation
650280 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
650281 289007 NOV - Notice of Violation
650281 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
650282 289007 NOV - Notice of Violation
650282 371337 CACP - Consent Assessment of Civil Penalty Comply/Closed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777578 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777579 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777580 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777589 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777590 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777591 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777592 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777593 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777594 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777595 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
777596 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
805316 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
805324 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
805325 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
820754 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
820755 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00
820756 371337 CACP - Consent Assessment of Civil Penalty COMP - Completed 2019-01-11 2019-01-11 $32,675.00 $32,675.00

For data sources see[8]

References