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37-125-21777

Well Details

Well ID: 37-125-21777
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Blaine Township
Operator Name: DALLAS ENERGY LLC
Well Pad ID:
Farm/Lease Name: JAMES NOBLE 033
License Status: Plugged and Abandoned
Spud Date: 1994-12-27
Permit Date: 1994-10-13
Well Type: INJECTION
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.175250
Longitude: -80.384222

For data sources see[1][2][3]

Well History

Date Event
1994-10-13 New Permit Application
1994-12-27 Performed Spud Operation
1995-01-17 Perforation
1995-02-17 Performed Stimulation
1995-02-19 Drilling Completion
1996-03-25 NEWLY DRILLED
2016-10-03 Begin Plugging
2016-11-03 Begin Plugging
2016-11-16 Finished Plugging
2019-03-05 Fully Plugged

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1995-02-17 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1996 PENNZOIL PROD CO 0.00 0 0.00 0 0.00 0
1997 PENNZOIL PROD CO 0.00 0 0.00 0 0.00 0
1998 PENNZOIL PROD CO 0.00 0 0.00 0 0.00 0
1999 PENNZOIL PROD CO 0.00 0 0.00 0 0.00 0
2000 PENNZOIL PROD CO 0.00 0 0.00 0 0.00 0
2001 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2002 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2003 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2005 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2006 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2007 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2008 EAST RESOURCES INC 0.00 0 0.00 0 0.00 0
2010 EAST RESOURCES MGMT LLC 0.00 0 0.00 0 0.00 0
2011 SWEPI LP 0.00 0 0.00 0 0.00 0
2012 SWEPI LP 0.00 0 0.00 0 0.00 0
2013 SWEPI LP 0.00 0 0.00 0 0.00 0
2014 SWEPI LP 0.00 0 0.00 0 0.00 0
2015 SWEPI LP 0.00 0 0.00 0 0.00 0
2016 SWEPI LP 0.00 0 0.00 0 0.00 0
2017 SWEPI LP 0.00 0 0.00 0 0.00 0

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2534587 Primary Facility 2016-11-02 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ has rig & equipment on site, getting ready to rig up.
2543854 Primary Facility 2016-11-08 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ pulled 5 joints of 4 1/2" casing, SD.
2543857 Primary Facility 2016-11-10 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Conserv pulling 4 1/2" casing.
2543858 Primary Facility 2016-11-15 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Conserv ran CBL on 7"casing & found several tight spots. Shot every 100 feet through the free areas based on CBL. Plan is to spot 1100 foot cement plug.
2543859 Primary Facility 2016-12-01 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ completed plugging, removed equipment, geaded, seeded and mulched location. Marker is buried.

For data sources see[7]

References