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37-125-22153

Well Details

Well ID: 37-125-22153
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Country: United States
State: Pennsylvania
County: Washington
Municipality: West Pike Run Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: W H WILSON 4
License Status: ACTIVE
Spud Date:
Permit Date: 2004-06-22
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.073080
Longitude: -79.976102

For data sources see[1][2][3]

Well History

Date Event
2004-06-22 New Permit Application
2004-08-30 Performed Spud Operation
2004-09-09 Drilling Completion
2006-03-03 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 CONSOL GAS CO 18430 365 0.00 0 0.00 0
2006 CONSOL GAS CO 7816.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 220.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 6365.18 365 0.00 0 0.00 0
2009 CONSOL GAS CO 5067.12 365 30.00 365 0.00 0
2010 CONSOL GAS CO 4,706.00 365 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 3,023.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 2,947.22 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 2,641.83 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 2,195.79 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 1,648.80 366 0.00 0 0.00 0
2017 CNX GAS CO LLC 1,898.00 365 0.00 0 0.00 0
2018 CNX GAS CO LLC 1,460.23 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2005 CONSOL GAS CO Brine 1,187.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2008 CONSOL GAS CO Brine 233.00 Bbl Brine or Industrial Waste Treatment Plt PA0026034
2009 CONSOL GAS CO Brine 77.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2009 CONSOL GAS CO Brine 22.00 Bbl Brine or Industrial Waste Treatment Plt PA0101508
2010 CONSOL GAS CO Produced Fluid 61.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2014 CNX GAS CO LLC Produced Fluid 44.00 Bbl INJECTION DISPOSAL WELL 34-059-24067
2015 CNX GAS CO LLC Produced Fluid 13.00 Bbl INJECTION DISPOSAL WELL 34-059-24067

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1371304 Primary Facility 2004-08-23 Routine/Complete Inspection No Violations Noted Wilson #4 is accessed and staked, but not begun so far as the bench. Access is properly constructed off of Woodland Rd.
1379577 Primary Facility 2004-09-21 Routine/Complete Inspection No Violations Noted Nippled wellhead, pits lined containing cuttings, topsoil stockpiled, haybales stockpiled, logs trimmed & piled.
1382840 Primary Facility 2004-10-06 Complaint Inspection No Violations Noted Well was in stage of development, fracing, rig up, dusty road, sump fluid within containment, and generally in the hustle of the motored equip. and rig work, thus a neighbor complained about the smells & dust. Nothing undue was noticed or noted and the main well work was over on this date with piping and restorations yet to do.
1388279 Primary Facility 2004-09-03 Drilling/Alteration No Violations Noted rig shut down, WOC, e/s ok
1442517 Primary Facility 2005-04-26 Routine/Complete Inspection No Violations Noted Bench well done except awaits repair from a stuck vehicle center stage of bench on restoration.
1442520 Primary Facility 2005-04-26 Routine/Complete Inspection No Violations Noted Some restoration started, bench work on equip. may or may not be complete.
2749283 Primary Facility 2018-07-06 Routine/Complete Inspection No Violations Noted On 7/6/18 an incident inspection was conducted of the WH Wilson 4 OG Well in response to a complaint concerning a possible unreported spill at a nearby well. The following was observed:

>>The well and associated equipment appeared to be in good condition with no noted issues. No violation.

For data sources see[7]

References