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Well ID: 37-129-00665 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: South Huntingdon Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: W R MAURER 670215 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.230667 | |
Longitude: -79.774833 |
Date | Event |
---|---|
1911-03-01 | Drilling Completion |
1911-12-30 | OLD WELL |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | COLUMBIA NATURAL RES INC | 382.00 | 21 | 0.00 | 0 | 0.00 | 0 |
1996 | CASTLE GAS CO INC | 584 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | CASTLE GAS CO INC | 321 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | CASTLE GAS CO INC | 323 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | CASTLE GAS CO INC | 282 | 348 | 0.00 | 0 | 0.00 | 0 |
2000 | CASTLE GAS CO INC | 327 | 351 | 0.00 | 0 | 0.00 | 0 |
2001 | CASTLE GAS CO INC | 306 | 304 | 0.00 | 0 | 0.00 | 0 |
2002 | VIKING RESOURCES CORP | 410 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | VIKING RESOURCES CORP | 396 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | VIKING RESOURCES CORP | 365 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | VIKING RESOURCES CORP | 387 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | VIKING RESOURCES CORP | 473.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | VIKING RESOURCES CORP | 374.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | VIKING RESOURCES LLC | 592.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2009 | VIKING RESOURCES LLC | 564.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | VIKING RESOURCES LLC | 389.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | VIKING RESOURCES LLC | 139.00 | 1 | 0.00 | 0 | 0.00 | 0 |
2012 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | DIVERSIFIED OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2177030 | Primary Facility | 2013-06-20 | Incident- Response to Accident or Event | Pending | The Department was notified of a natural gas release at the above referenced location. The Department arrived on site and immediately smelled gas when getting out of truck. The Department utilized a PID Meter for gas readings/safety reasons. Natural Gas was leaking from a Viking Gas Well according to Jerry Kurfcheck from Atlas. The gas was leaking at the well head from a 4 inch casing. Atlas placed a saddle clamp on the casing to fix the leak. The odor dissipated after the leak was fixed. The Gas Well head appeared to be in bad condition and needs repaired. Recommendations will be made to the responsible party and a permanent fix will be needed. |
For data sources see[6]