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Well ID: 37-129-00667 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: Sewickley Township | |
Operator Name: CHEVRON APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: D M CURRY | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.234786 | |
Longitude: -79.787361 |
Date | Event |
---|---|
1902-08-27 | Drilling Completion |
1902-12-30 | Old Well |
2017-06-29 | Begin Plugging |
2017-07-17 | Finished Plugging |
2019-05-16 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | COLUMBIA NATURAL RES INC | 34.00 | 21 | 0.00 | 0 | 0.00 | 0 |
1996 | CASTLE GAS CO INC | 427 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | CASTLE GAS CO INC | 245 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | CASTLE GAS CO INC | 235 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | CASTLE GAS CO INC | 217 | 348 | 0.00 | 0 | 0.00 | 0 |
2000 | CASTLE GAS CO INC | 268 | 351 | 0.00 | 0 | 0.00 | 0 |
2001 | CASTLE GAS CO INC | 239 | 304 | 0.00 | 0 | 0.00 | 0 |
2002 | VIKING RESOURCES CORP | 346 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | VIKING RESOURCES CORP | 316 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | VIKING RESOURCES CORP | 275 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | VIKING RESOURCES CORP | 22 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2017 | CHEVRON APPALACHIA LLC | Synthetic Liner Materials | 4.43 Tons | LANDFILL | 100172 |
2017 | CHEVRON APPALACHIA LLC | Drilling Fluid Waste | 38.30 Bbl | LANDFILL | 100663 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2539651 | Primary Facility | 2016-11-29 | Complaint Inspection | No Violations Noted | At the time of inspection the well appeared to be drilled and equipped for production. The well apparatus appeared to be in sound condition. The well tag was present. No observation of accelerated erosion or sedimentation. |
2613470 | Primary Facility | 2017-07-10 | Routine/Complete Inspection | No Violations Noted | At the time of inspection the Operator was actively plugging the well. The coil tubing rig was on site and placed on secondary containment. No observation of accelerated erosion or sedimentation in relation to the well pad or access road. |
2615760 | Primary Facility | 2017-07-17 | Incident- Response to Accident or Event | Violation(s) Noted | Response to spill reported to the Department on 7/16/2017 at 8pm. The Operator indicated that approximately 10 barrels of concrete was lost under the secondary containment at 6pm. The Operator indicated that they were pumping concrete into the production casing and lost circulation. The Operator observed concrete on the edge of the well pad. Plugging activity was stopped. The Operators inspection revealed concrete was returning to the surface via the annular casing under secondary containment. The well permit was on site. ERP onsite. The PPC plan was on site. SDS on site. E& S plan was on site. Operator representatives onsite during inspection B.A Lambie, Ronnie Venghaus and Mark Manning. The Departments inspection confirmed that concrete was last lost to the well pad and appeared to be under the containment. Waters of the Commonwealth were not impacted. The cement solidified prior to leaving the perimeter controls. The Department observed two open top tanks. One of the tanks had less than 2 feet of freeboa |
2616547 | Primary Facility | 2017-07-19 | Follow-up Inspection | In Compliance with Schedule | Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator removed the secondary containment in the area of the release. The impacted area appeared to be remediated, the concrete removed was placed on containment awaiting disposal. The Operator indicated that confirmation samples were collected. The attached photo contains flags indicating the confirmation sample locations. The open top tanks located on site had more than 2 feet of freeboard. |
2625428 | Primary Facility | 2017-08-14 | Follow-up Inspection | In Compliance with Schedule | Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator was not actively working on the site during the inspection. Secondary containment removed and placed in two open top roll off boxes. The contents of an additional three roll off boxes also located on site could not be verified. Well plugged. The berm located on two sides of the well site appeared to have small erosion rills but no evidence that suggests the sedimentation is leaving the location or impacting waters of the Commonwealth. The Department recommends the Operator continue to monitor the site weekly and after significant precipitation events. |
2635228 | Primary Facility | 2017-09-11 | Follow-up Inspection | In Compliance with Schedule | Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator was not actively working on the site during the inspection. The site appears to be unchanged since 8/14/2017 follow up inspection. Well plugged. Roll off boxes with containment on site. Temporary erosion and sedimentation BMPs in place and functioning. The Department recommends the Operator continue to monitor the site weekly and after significant precipitation events. |
2642481 | Primary Facility | 2017-10-02 | Follow-up Inspection | In Compliance with Schedule | Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator was not actively working on the site during the inspection. The Operator has removed four open top roll off boxes from the well site. One new roll off boxes has been delivered to the site and one closed, residual waste box remains on site. Well plugged. Temporary erosion and sedimentation BMPs in place and functioning. The Department recommends the Operator continue to monitor the site. |
2654643 | Primary Facility | 2017-10-31 | Administrative/File Review | In Compliance with Schedule | Administrative inspection. On 10/31/2017 the Department received the Operators Site Characterization and soil excavation report associated with the release of cement which occurred on7/16/2017. |
2667578 | Primary Facility | 2017-12-05 | Compliance Evaluation | No Violations Noted | Well plugged. No monument observed. Site regraded, seeded and mulched. Temporary E&S BMP site sox appears to be installed and functions as designed. The Department recommends that the Operator continue to monitor the site until the site is returned to previous use or 70% uniform vegetative coverage is established. The Violation associated with inspection report 2615760, relating to the release of cement, have been corrected and the Operator has complied with the Departments spill policy. |
758513 | Primary Facility | 1991-01-24 | Routine/Complete Inspection | No Violations Noted | E&S OK; NO TANK |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2615760 | 791904 | 2017-07-17 | 2017-12-05 | 78.57(a) | Environmental Health & Safety | Operator failed to control. |
2615760 | 791905 | 2017-07-17 | 2017-12-05 | 78.56(a)2 | Environmental Health & Safety | Operator failed to maintain 2 feet of freeboard. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
791904 | 356552 | NOV - Notice of Violation | 2017-12-05 | ||||
791905 | 356552 | NOV - Notice of Violation | 2017-12-05 |
For data sources see[7]